IT WORKS!..kinda
#1
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IT WORKS!..kinda
Well the good news is the kit is in! I turned the key and first try it ran...like ****. It idles fairly good and I'm showing 17-20 on the vacuum and 40-50ish psi of oil pressure on a cold start. So YAY! no nicked oil pickup! I have fought this stupid kit every single step of the way!
My biggest problem is the stock exhaust will not line up with the downpipe. I couldn't get the bolts loose from the manifold so I took it off at the mid pipe. I bolted the downpipe to the midpipe and reinstalled. Now I can't bolt the downpipe to the turbo! It sits too far back and too far to the left (when looking from the front of the car). I think it has something to do with that bracket holding it to the trans, seems like its holding it back from coming all the way up where I want it.
I started it up without the downpipe connected and it runs, will rev but is very stumbly and my boost gauge shows no boost. Also my BOV didn't open. I'm assuming this is because of the wastegate not being sealed and the o2 sensor not being in the right way. Am I right?
My second problem is my jackson racing s/c (EVIL!!!) air filter is friggen HUGE and wont let the intake tuck in the corner, so I had to leave it too high and now my hood wont close.
All in all, I'm happy as hell its in and will run. The whole 30 seconds I had it running made me smile as I heard the turbo spool up. But I'm still in trouble, so hopefully you guys can help me out. Thanks.
My biggest problem is the stock exhaust will not line up with the downpipe. I couldn't get the bolts loose from the manifold so I took it off at the mid pipe. I bolted the downpipe to the midpipe and reinstalled. Now I can't bolt the downpipe to the turbo! It sits too far back and too far to the left (when looking from the front of the car). I think it has something to do with that bracket holding it to the trans, seems like its holding it back from coming all the way up where I want it.
I started it up without the downpipe connected and it runs, will rev but is very stumbly and my boost gauge shows no boost. Also my BOV didn't open. I'm assuming this is because of the wastegate not being sealed and the o2 sensor not being in the right way. Am I right?
My second problem is my jackson racing s/c (EVIL!!!) air filter is friggen HUGE and wont let the intake tuck in the corner, so I had to leave it too high and now my hood wont close.
All in all, I'm happy as hell its in and will run. The whole 30 seconds I had it running made me smile as I heard the turbo spool up. But I'm still in trouble, so hopefully you guys can help me out. Thanks.
#3
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well the car ran perfectly fine before I put the turbo in. I will wait to judge until I get the downpipe on the turbo tho, I need to drive it to work tuesday so hopefully all goes well.
#4
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Well I took it for a drive....HELL YEAH! its REALLY loud with just a down pipe, but from the gauges and noises it made I didnt hear anything ill sounding. I only went to 3 p.s.i. so I wouldnt hurt anything. And thanks to my crappy jrsc air filter the AFM wont fit, so I had to take the hood off.
One thing that does sound strange is the turbo spools up, but I dont enter boost, and sounds like it slowly winds down after I let off the gas. Should the BOV open so it doesnt do that or is this normal? It is a smooth wind down, not like a turkey gobble (but I have never heard that noise before).
And I painted my manifold with high temp paint when I first got it some 4 months ago to keep the rust down, and yeah it just burned right off lol. Good thing it wasn't intended to stay, but I do regret it as now it smokes like crazy. So with all hope it will make it to work tommorow and I can install my 1.8 injectors and get working on the emanage. Only thing holding me up with that is the dumb support tool. Winrar isnt working right so I need to locate it somewhere else.
One thing that does sound strange is the turbo spools up, but I dont enter boost, and sounds like it slowly winds down after I let off the gas. Should the BOV open so it doesnt do that or is this normal? It is a smooth wind down, not like a turkey gobble (but I have never heard that noise before).
And I painted my manifold with high temp paint when I first got it some 4 months ago to keep the rust down, and yeah it just burned right off lol. Good thing it wasn't intended to stay, but I do regret it as now it smokes like crazy. So with all hope it will make it to work tommorow and I can install my 1.8 injectors and get working on the emanage. Only thing holding me up with that is the dumb support tool. Winrar isnt working right so I need to locate it somewhere else.
#6
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Well I have a new big problem. Once again the jrsc has screwed it up. The throttle body has that funky anti freeze coupling on the bottom. Under boost the bottom of it leaks. My question is how should I fix it? I'm pretty sure there is still some gasket material on the throttle body, I tried to sand it off but aparently I didnt do a good enough job. On the stock TB is there a gasket for this setup or is it all machined surfaces? And on a side note...why the hell does the antifreeze go over there?! So now my car has no hood, a raised intake and leaks antifreeze...but it also has turbo powah!
Should add, the jrsc relocates the TB to the drivers side and puts a dummy TB is put in the stock location. The person who installed the jrsc used a supplied gasket which hardened and when I tried to remove it broke apart.
Should add, the jrsc relocates the TB to the drivers side and puts a dummy TB is put in the stock location. The person who installed the jrsc used a supplied gasket which hardened and when I tried to remove it broke apart.
#7
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Well after a close inspection I somehow missed that there is a gasket between them. Checking the dummy TB I found the gasket, which was hidden under a jackson racing orange gasket. Fingers crossed for the drive to work tommorow
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