Dropped Valve Head Repair
36 Attachment(s)
4G63 Dropped Valve Head Repair
The Subject head is a 1G 6 bolt head. This head had extensive work done to it and would cost way more to replace than repair. The head was loaded with SuperTech +1mm valves, and duel valve springs and Ti retainers. How the head looked when I received it. https://www.miataturbo.net/attachmen...ine=1340816317 A closer look at #4 cylinder, the one that dropped the valve. https://www.miataturbo.net/attachmen...ine=1340816317 Yes it looks pretty beat. But it is fixable. First thing to do is disassemble the head and get a parts list going. At first look, I thought the 4 valves in the #4 cylinder would be the only ones needing replaced. It turned out only 4 valves of the 16 could be used. https://www.miataturbo.net/attachmen...ine=1340816317 The SuperTech duel springs and Ti retainers tested fine and will be used. About half of the Ti retainers had be rubbed on. https://www.miataturbo.net/attachmen...ine=1340816317 At this time it was decided to install bronze guides, to replace the stock appearing cast iron guides. https://www.miataturbo.net/attachmen...ine=1340816317 The bronze guides installed. https://www.miataturbo.net/attachmen...ine=1340816317 Once the head was cleaned, a couple small cracks were found in #1 cylinder. https://www.miataturbo.net/attachmen...ine=1340816317 The seats were cut out https://www.miataturbo.net/attachmen...ine=1340816317 Then the head was pressure tested, using 35psi in the water jacket. The head did not leak. So work progressed by removing the 4 seats in #4 cylinder. https://www.miataturbo.net/attachmen...ine=1340816317 New counter bores were cut, and oversized inserts were installed. https://www.miataturbo.net/attachmen...ine=1340816317 Some grinding, polishing and blending was done to smooth out some of the damaged area in the combustion chamber. Next was to mark the spots to be welded. https://www.miataturbo.net/attachmen...ine=1340816317 What it looked like once back from the welder. https://www.miataturbo.net/attachmen...ine=1340816317 Also to note is the spark plug inserts were installed in cylinders #1 and #4 before welding. From this point a bit more blending was done to smooth out the welds and a full valve job was performed. As the seats were cut, https://www.miataturbo.net/attachmen...ine=1340816317 Valve tip height was checked and set to the proper specs. https://www.miataturbo.net/attachmen...ine=1340816317 Spring installed height was measured and set to 1.550 @ 85lbs https://www.miataturbo.net/attachmen...ine=1340816317 New 3g HLAs were installed, along with the followers and cams. https://www.miataturbo.net/attachmen...ine=1340816317 Bottom of the head. https://www.miataturbo.net/attachmen...ine=1340816317 Close up of #4 cylinder after repair. https://www.miataturbo.net/attachmen...ine=1340816317 Head thickness after repair and rebuild. 5.159 Head build # BBB 744 |
congrats on slightly better pictures with the new camera!
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^ lol
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Well some of the pics were taken with the new camera, some with the old one and a few with my cell.
But I am trying and learning. |
no, they are MUCH better. and very appreciated.
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