2 Attachment(s)
Been on the dyno today.
Made more power and torque. Very happy with it now. A MASSIVE thanks to Dan at ardler automotive for checking the whole map over of me again. Rev limit lowered to 7k Hopefully it last more than 4 days this time. Attachment 184704 Attachment 184705 If any of you are on Instagram follow me on there for more pics Username: connorhorton |
That's...uh...a funny looking torque curve.
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Holy shit, it's just like looking out the window of my house (a mountain).
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not loading for me. i hate photobucket.
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So the car went on the dyno again today, it instantly made better power and needed work to the fuel map (especially in boost) to get it where it needs to be.
The strange torque curve comes from the same flaws in the original turbo setup where it just can't make the boost at the top end. It does however make for a lovely flat power graph at the top (I'd much rather have flat torque to redline but not many people run big enough turbos on stock engines). It's also emphasised by the way that the DynaPack auto-scales it's axis, which makes small changes look rather… large. All in all - it's back on the road and the iMessage from Connor a short while ago that said "It's sooo much faster", it's amazing what an extra 20bhp can do :-) Daniel |
It's nice to see the dyno runs start at a nice low RPM.
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With that torque curve you should have set the redline at 6000 rpm. He's got no business revving it out any higher than that with that clogged exhaust. All that it will do is make excess heat and cylinder pressure above there, and maybe cost him another engine.
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After seeing that dyno I would be concerned the cause of the original failure still lurks within the new motor. That type of torque fall off means you got one hell of a restriction somewhere. Restrictions like that cause cylinder temps to really skyrocket and lead to detonation.
I would pull the exhaust and dyno with just a downpipe and see if anything changes. |
Diesel swap?
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The cam timing is off. Im calling it. Im sure its been said before, but seriously, the mechanical timing is advanced a tooth somewhere.
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So...what PSI is that at?
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That's fucked. It's dropping torque worse than a stock msm.
It's gonna blow again. |
The exhaust really isn't very restrictive at all. The down pipe is the standard Hks on that's been chopped and made to be more free flowing but it does have a pretty sharp angle off the turbo so that must be a restriction I suppose.
Still at 13psi. Cam timing is not off. Torque really doesn't feel like it's dropping off that bad I'm sure dan will answer with a more technical answer |
There is a problem. Look at all the dyno plots posted of our cars, none of of them look like yours.
None of them choke down like that. Even the ones with stock exhaust don't drop to 100tq @ redline |
omg, someone post the actual images here. photobucket never works for me.
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this is his torque curve: /\
literally drops from 200 too 100 by redline. |
Originally Posted by Horton
(Post 1165826)
Torque really doesn't feel like it's dropping off that bad
Are you using a catalytic converter and stock muffler? |
Originally Posted by 18psi
(Post 1165830)
this is his torque curve: /\
literally drops from 200 to 100 by redline. I cant see how 150rwhp once it FINALLY spools to redline can feel good... Typically when one makes 200rwtq, you'd expect at least 230rwhp. What turbo is this? |
No cat at all. Straight pipe from the turbo back to a single straight through box at the rear. All of it 2.5"
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Originally Posted by 18psi
(Post 1165830)
this is his torque curve: /\
literally drops from 200 too 100 by redline. It's making 10wtq more at redline than my motor did... WHEN MY MOTOR WAS N/A. http://forum.miata.net/vb/picture.ph...&pictureid=994 |
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