lol at weight savings.
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Honestly, I thought I remembering reading that the piece had something to do with helping with vibrations and what not...definetly nothing to do with the tb.
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I'm willing to bet the rigidity of the IM stays the same with or without the brace.
never heard of any failure directly related to it, and im sure more than 50% of the m.net members have their brace removed. |
Originally Posted by Braineack
(Post 396690)
I'm willing to bet the rigidity of the IM stays the same with or without the brace.
never heard of any failure directly related to it, and im sure more than 50% of the m.net members have their brace removed. In order to help any with rigidity it needs to have tension on it, which it does not. |
anyone measured the amount the intake manifold moves relative to the block at all RPM conditions? because it probably does a little. And aluminum SUCKS at fatigue resistance. just a mm or two of shake will break stuff fast.
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the dsms have a very similar brace which i removed from my car with no issues at all, however my buddy removed it and his manifold literally fell off during a hard launch.
i think the only difference was that he had his coils mounted to the manifold like they are stock and i had cops. maybe the extra weight on it did it? it left the flange on the head and was hanging from throttle cable and plug wires. |
Removed the damn thing from our integra as well when I redid the head. No issues there either.
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Originally Posted by Braineack
(Post 396690)
I'm willing to bet the rigidity of the IM stays the same with or without the brace.
never heard of any failure directly related to it, and im sure more than 50% of the m.net members have their brace removed. |
Originally Posted by 1slowna
(Post 396721)
the dsms have a very similar brace which i removed from my car with no issues at all, however my buddy removed it and his manifold literally fell off during a hard launch.
I think the only difference was that he had his coils mounted to the manifold like they are stock and i had cops. Maybe the extra weight on it did it? It left the flange on the head and was hanging from throttle cable and plug wires. |
I removed it on all 3 of my DSMs the first time I ever had to do anything underneath it. Never looked back.
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K. If you drive your shit hard, leave it in.
So everyone here, go ahead and take it out. And how do you not see a correlation between the intake manifold brace and those bolts backing out? Leave the engineering to the engineers, not your puny little brain. |
After just watching a video of Savington on the track, and him saying he doesn't have it installed, really leads me to believe that it's going to be just fine without it.
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Originally Posted by crashnscar
(Post 397001)
K. If you drive your shit hard, leave it in.
So everyone here, go ahead and take it out. And how do you not see a correlation between the intake manifold brace and those bolts backing out? Leave the engineering to the engineers, not your puny little brain. BTW - Like I told Sav, I'm not an engineer, or an engineering student, or anything like an engineer. I don't think that makes my brain "puny", kthx. :2cents: |
Originally Posted by RotorNutFD3S
(Post 397007)
After just watching a video of Savington on the track, and him saying he doesn't have it installed, really leads me to believe that it's going to be just fine without it.
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Originally Posted by Savington
(Post 397035)
I want it in, though. I tried to leave it in but I need to redo my oil cooler lines to make it fit. If you have room for it, it should be installed.
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Oil filter relocation...problem solved.
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Originally Posted by RotorNutFD3S
(Post 397007)
After just watching a video of Savington on the track, and him saying he doesn't have it installed, really leads me to believe that it's going to be just fine without it.
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mine doesn't fit because of the intake manifold spacer gasket. I need to put one on the bottom of the bracket to space it out accordingly.
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Be careful with the intake manifold spacer and no brace. I ran this way on my NA track car. After a lot of abuse on track, three of the intake manifold studs broke, the intake started to suck in air and burned out the #4 piston.
I am now running with the stock intake gasket and the brace. The engine really moves around a lot at 7,000 rpm. |
Originally Posted by kotomile
(Post 397013)
I suppose there could be a resonance, hadn't thought of that. Is the theory that Emilio's TB screw backed out due to the sustained vibration?
BTW - Like I told Sav, I'm not an engineer, or an engineering student, or anything like an engineer. I don't think that makes my brain "puny", kthx. :2cents: |
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