EGO Correction PID
My '99 has FF 640s and a non-return fuel system. As such, I do get some pretty wild variation on EGO, especially when idling and especially dependent on under-hood temps. In order to deal with it I'm using what I consider fairly aggressive PID correction for my EGO. I found that the fastest, precise, correction seems to happen when using the EGO delay table, meaning that the reaction time changes based on MAP/RPM.
My settings are: P: 30 I: 65 D: 40 I figured out the delay at multiple conditions by changing the VE while driving steady-state and measuring in the log how long it takes for the change in AFR to show up. The delays actually seem fairly long to me- from about 700ms in idle and around 50ms (which is an estimate, not measured) in boost at 6krpm. Is anybody else using this? With what level of success? |
The EGO delay is largely based on MAP/TPS. With MAP ~30 I get a delay of about 2s, at ~80-90 it's more like 800-900ms.
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