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-   MEGAsquirt (https://www.miataturbo.net/megasquirt-18/)
-   -   idle perfect, then suddenly full rich on afr (https://www.miataturbo.net/megasquirt-18/idle-perfect-then-suddenly-full-rich-afr-60480/)

miatauser884 09-17-2011 08:19 PM



im having an issue where my car is running perfect at 14.5 afr, then suddenly pegs rich for a couple seconds, then recovers. it also happens while driving and feels like a moment of hesitatio. nothing in the log shows anything wrong. i noticed it with my diypnp, but it is more pronounced on ms3. probably due to better idle control with ve table.

if a coil dropped out, would it be enough to send afr to full rich on wbo2? does coil trigger record in datalog? i want to see if it happens on the same trigger every time.

Reverant 09-18-2011 03:02 AM

It does sound like a coil going bad. I was able to find which one was bad on mine using the 4 widebands. 2 & 3 were going full rich when it happened.

curly 09-18-2011 04:09 AM

Pull a plug, see if it does the same thing, my guess is not. My car will damn near stall if it looses 2 cylinders. You'd know for sure.

Braineack 09-18-2011 10:42 AM

(Posting from my phone.)

Post the log. There's no cause that I can find in the megasquirt. The map rises a little just before the event. Then the rpm droops as the airs dump to 10:1.

Is it constant? I wonder off you can suit on the coil bench test mode for a few minutes and see if you can pinpoint a coil that's missing.

miatauser884 09-18-2011 10:52 AM

It seems kinda random. It's very obvious when it happens at idle, and I cn feel it when it happens while driving. I've got a few spare cops. Before I change the plugs I'm going to let it idle and replace one coil at a time to see if it disappears. I'll mess with the coil bench test mode and see what I see. The log is too big to post, I'll try to take another.

miatauser884 09-18-2011 12:57 PM

2 Attachment(s)
I changed the COPs one by one, and still get the issue. I did the trigger log,and when it happened the y axis increased significantly. I'm not really sure what I am looking at though. I've uploaded a datalog that shows it happening a few times.

miatauser884 09-19-2011 07:13 PM

Update: I replaced the spark plugs with NGK 4091 (resistor-less). Unfortunately this random rich condition is still there.

I used the realtime logger and did notice an increase in the pulsewidth when this happened.

At first I was thinking that maybe the fuelpump was receiving a voltage spike. However, this would not be logged in tunerstudio as an increase n pulsewith.

Possible culprits:

CAS: not sure how, but it is responsible for synchronization of fuel and spark. Hopefully one of the smarter individuals will chime in on this. I have a trigger wheel to install in the CAS, but I'm unaware if this is a solution for a worn or failing CAS since I am unsure about what actually fails when they go bad. I do have a spare CAS though. If this sounds like it could be a culprit, then please let me know.

Software: Something in software not configured properly. Always a possibility, but I have gone over everything pretty carefully looking for something that seemed like it could be a possibility.

Firmware: I think this is a possibility. maybe the firmware didn't write 100% correctly. Although the issue seems random. Today it seemed like it followed the same pattern as it did the day before. I'm concerned that something is going on behind the scenes that isn't showing up on screen. For instance. My CL idle dash light isn't on all the time while idling, yet all the parameters suggest that it should be on. It turns on, stays lit for a while, then turns off all while the idle remains constant. This makes me wonder if ASE or WUE is kicking in randomly for a second and then turning off. this would easily cause a momentary rich condition.

Hardware: Not likely. I don't see what could randomly send a signal to momentarily increase injector pulsewidth and then go away.

Ignitor: spark could be dropping out, but I would expect PW to stay the same. Realtime display suggest the pulswidth increased by ~ 12% going form 1.4ms to 1.6ms

I think I am going to upgrade to the pre alpha 1.1 version 14. I think there is enough difference in the software that if it were firmware related, then it would probably be removed. I guess I could reflash the current firmware, but where is the fun in that. Part of the reason I upgraded to MS3 is because I am a firmware junky.

I'm going to hold off doing anything until I get a few responses/suggestions

Braineack 09-19-2011 07:14 PM

2 Attachment(s)
The log below, the PW follows the GVE (fuel map VE %) as the MAP increases. I dont think it's enough to be causing the dip, the dip happens a few moments after the fact.

really seems like the coils are dropping out.

there's a couple of instances on your log file where the AFRs dont drop rich, but the RPMs and MAP become really unstable.



https://www.miataturbo.net/attachmen...1&d=1316474510

miatauser884 09-19-2011 07:18 PM

??? SD card??? Then what?

Braineack 09-19-2011 07:24 PM

one thing I find odd the the idle valve seems to be doing nothing... the entire log it's just slowly opening more and more.

miatauser884 09-19-2011 07:25 PM

If that is the case, then what are your thoughts about the CAS?

Braineack 09-19-2011 07:31 PM

its not losing sync.

miatauser884 09-19-2011 07:32 PM


Originally Posted by Braineack (Post 773192)
one thing I find odd the the idle valve seems to be doing nothing... the entire log it's just slowly opening more and more.

Bad idle valve. I found it odd that my car wasn't in closed loop idle while idling.

About to log to SD card

miatauser884 09-19-2011 08:49 PM

sending you a log. Go to 175s. Good pic of what's happening. Looks like I have been chasing a ghost. Something else going on.

miatauser884 09-19-2011 09:45 PM

I think I have to accept the fact that my car has a HG leak. Too much water is coming of the tailpipe while idling. I end up with a small puddle, and just before I finished I started to see little puffs of white smoke out of the tailpipe. I think the HG stop leak I had in there keeps it at bay if I am driving it regularly and circulating the coolant. For kicks I decide to run it a 4k rpm for a while to circulate the coolant. Low and behold that mysterious issue I had disappeared.

Hopefully it won't take too long to change the HG.

After a lot of googling it seems that this water issue is not uncommon during periods with a lot of moisture in the air and idling near stoich. I don't know. I'm going to button everything up and just start driving it. To me, the instability in the log would not lead to such a rich afr.

lordrigamus 09-21-2011 07:31 AM

Doesn't seem like anything on the log would be triggering it but are the accel enrichments randomly kicking in, maybe?

(edit) Nevermind. Just reviewed your log and the accels never kicked in.

miatauser884 09-21-2011 08:14 AM

I think I found the culprit last night.

I think it is the VICS vacuum lines. The VICS solenoid was bypassed on the dyno because the tuner said it actually hurt performance when they were activated at 5200 rpm. The lines going into the solenoid were plumbed into a t fitting with the 3rd end capped. This results in the manifold being directly tied to the vacuum pod behind the throttle body.

It appears that the vac lines are slightly too big for the ports. When enough vaccuum is pulled, air is able to momentarily leak past the rubber tube, but then once the vac is reduced the seal is sufficient to discontinue the leak. Vac builds back up and it happens again. However, there doesn't seem to be an exact amount of vac that causes the leak so it appears random. I'm going to get new vac lines today, and hook up VICS again. Maybe I didn't have them working right on the dyno. Peopel seem pretty confident that it helps low end torque a little. Not sure if my cam gear has a negative effect on the VICS.

Braineack 09-21-2011 08:27 AM

thats because VICs should be ON until 5300 or so.

miatauser884 09-21-2011 09:50 AM

settings should be 0 for start, then 1 for active at the desired rpm?

Braineack 09-21-2011 10:20 AM

should be:

trigger 1 | 0

rpm > 5300 hysterisis 100

so solenoid is powered below 5300.


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