Warning to other newbies: baro correction and lumpy idle
There were a couple of posts from people w/ the same issues I had, I'm running V3.0 MS1 w/ Hi-res code.
I just found my problem that was causing: -Idle bouncing between lean and rich -Starting out cruising at 14 AFR and going progressively lean over time -A VE table that looks like the Andes -Idling (when it wasn't bouncing) at 10.5 AFR no matter what I did to idle cells Turns out "constant baromtric correction" got switched on at some point (I don't have a second MAP sensor), it must have been picking up noise and f'ing up the whole works. I checked thru my datalogs, and barometric correction was all over the place, between 77% and 135% :eek5: It's amazing that the car ran as well as it did :) |
Thanks for the heads up.
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