GODDAMNMOTHERFUCKINGSHIT. (I fixed my misfire)
#1
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GODDAMNMOTHERFUCKINGSHIT. (I fixed my misfire)
I am so amazingly pissed off right now I'm temped to drive my car into the Pacific Ocean.
Since the initial install, I've been plagued by misfire under high load. Seems like it only happens when I'm in high boost- if I'm just accelerating slowly in 1st or 2nd I can take it to redline with no problems. So I don't know if it's rate of change of if it's really related to boost.
When it happens, the tach drops momentarily (tach is driven by the ignitor) and in the logs it registers as a seemingly random RPM value- sometimes a dip, sometimes a huge spike.
I've tried:
1- Upgrading to HR10G
2- Downgrading to 028y4
3- Replacing coils, wires, and plugs (gapped to .028")
4- Laying a .1uf car across JS8 and GND
5- Replacing said cap with a .47uf
6- Replacing the CMP input circuit with an optoisolator
7- Replacing both the CMP and CKP input circuits with a dual comparator circuit that Abe designed
8- Installing a 1k resistor between +12 and the black/white wire at position 2I of the stock harness
About the only thing I haven't done is install a PCPro...
[/rant]
Is nobody else having this problem?
Since the initial install, I've been plagued by misfire under high load. Seems like it only happens when I'm in high boost- if I'm just accelerating slowly in 1st or 2nd I can take it to redline with no problems. So I don't know if it's rate of change of if it's really related to boost.
When it happens, the tach drops momentarily (tach is driven by the ignitor) and in the logs it registers as a seemingly random RPM value- sometimes a dip, sometimes a huge spike.
I've tried:
1- Upgrading to HR10G
2- Downgrading to 028y4
3- Replacing coils, wires, and plugs (gapped to .028")
4- Laying a .1uf car across JS8 and GND
5- Replacing said cap with a .47uf
6- Replacing the CMP input circuit with an optoisolator
7- Replacing both the CMP and CKP input circuits with a dual comparator circuit that Abe designed
8- Installing a 1k resistor between +12 and the black/white wire at position 2I of the stock harness
About the only thing I haven't done is install a PCPro...
[/rant]
Is nobody else having this problem?
#2
I had the same issue until i gapped my plugs down to .025. Not sure if it is just the '99 coils or the BKR7E's i'm running but without gapping them down from .035-.028-.025 I was having issues.
I take it you don't have this issue when running the car to redline staying out of boost?
Are you running COPs yet?
I take it you don't have this issue when running the car to redline staying out of boost?
Are you running COPs yet?
#4
Throw your MSQ and a datalog into a zip file and post it... we'll take a look and see what we can see.
I had the same problem and it ended up being my ACCEL ENRICHMENT was kicking in and throwing an extra ****-ton of fuel. You could quick-like post a screenshot of you ACCEL ENRICHMENT PAGE4 in the BASIC SETTINGS window so I could rule it out.
I had the same problem and it ended up being my ACCEL ENRICHMENT was kicking in and throwing an extra ****-ton of fuel. You could quick-like post a screenshot of you ACCEL ENRICHMENT PAGE4 in the BASIC SETTINGS window so I could rule it out.
#5
I had this issue as well. Over time, I have done 3 things to try to address it, but didn't keep track of what helped, unfortunately. It's gone now though.
1.) Raised over boost protection a bit higher. I was getting brief boost spikes that put me close to the over boost I had input, which was causing issues. I now put over boost protection at ~5-8kPa above my peak anticipated boost.
2.) Ran an extra ground from the MS to the grounding point on the engine. This helped many issues, including noise in signals, and some misfires under rapid entry into boost
3.) Swapped stock plugs for the BKR7Es, but haven't seen a need for gapping them lower quote yet, as I'm only running 9psi.
1.) Raised over boost protection a bit higher. I was getting brief boost spikes that put me close to the over boost I had input, which was causing issues. I now put over boost protection at ~5-8kPa above my peak anticipated boost.
2.) Ran an extra ground from the MS to the grounding point on the engine. This helped many issues, including noise in signals, and some misfires under rapid entry into boost
3.) Swapped stock plugs for the BKR7Es, but haven't seen a need for gapping them lower quote yet, as I'm only running 9psi.
#6
I'd suggested pulling out the caps in the OEM circuit I'd posted, which I imagine will do the trick - but while for me it SEEMED boost dependant, I'm not sure it was.
That's a good point, I've had SO many problems which turned out to be accel enrichment which I thought was something else each of the times....
1) Yeah, though that's obvious from the logs. This isn't that, if it's what I've seen, since the tach will do funny things, the logs will do stuff like read 18,000 RPM
2) I did this two, tons of wire. Didn't help me, so I took it out.
3) I'm running 7's now. How would that help you, though??
Anyway, I had gapped mine small long ago when I doubted my coils, as usual, having 5 problems it wasn't obvious what fixed what, then.
When the toyo COP set up, I went back up to 0.35, and I have little doubt I could run 40 or 45 without issue, those things are amazing, even at 15 psi.
1.) Raised over boost protection a bit higher. I was getting brief boost spikes that put me close to the over boost I had input, which was causing issues. I now put over boost protection at ~5-8kPa above my peak anticipated boost.
2.) Ran an extra ground from the MS to the grounding point on the engine. This helped many issues, including noise in signals, and some misfires under rapid entry into boost
3.) Swapped stock plugs for the BKR7Es, but haven't seen a need for gapping them lower quote yet, as I'm only running 9psi.
2.) Ran an extra ground from the MS to the grounding point on the engine. This helped many issues, including noise in signals, and some misfires under rapid entry into boost
3.) Swapped stock plugs for the BKR7Es, but haven't seen a need for gapping them lower quote yet, as I'm only running 9psi.
2) I did this two, tons of wire. Didn't help me, so I took it out.
3) I'm running 7's now. How would that help you, though??
Anyway, I had gapped mine small long ago when I doubted my coils, as usual, having 5 problems it wasn't obvious what fixed what, then.
When the toyo COP set up, I went back up to 0.35, and I have little doubt I could run 40 or 45 without issue, those things are amazing, even at 15 psi.
#7
1) Yeah, though that's obvious from the logs. This isn't that, if it's what I've seen, since the tach will do funny things, the logs will do stuff like read 18,000 RPM
2) I did this two, tons of wire. Didn't help me, so I took it out.
3) I'm running 7's now. How would that help you, though??
2) I did this two, tons of wire. Didn't help me, so I took it out.
3) I'm running 7's now. How would that help you, though??
2) The later cars have more grounds to begin with. The 1.6 cars are sorely lacking, and can benefit from more grounds.
3)The 7's I run now are factory gapped slightly lower than the stock plugs, IIRC, which would help.
#9
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Ok, lots and lots of ideas here...
1- It ain't accel fuel. First, I'm on TPS accel and second, accel fuel wouldn't cause my tach to drop out.
2- During the original install I ran two additional 16ga grounds direct to the head. Trust me, it's well-grounded.
3- Overboost... Interesting- I'll try disabling it.
4- Dwell- I've tried between 4.5 - 5.5ms running, no difference. (stock igniter and coils)
5- Plugs: Tried BKR7E at .035" and IFR8H at .028" with no difference. Again, a genuine misfire wouldn't affect the tach. I guess I can re-gap my 7Es to .02" before I re-install 'em.
6- Abe, I just nixed the capacitors, and will retry after I get HR code re-loaded.
1- It ain't accel fuel. First, I'm on TPS accel and second, accel fuel wouldn't cause my tach to drop out.
2- During the original install I ran two additional 16ga grounds direct to the head. Trust me, it's well-grounded.
3- Overboost... Interesting- I'll try disabling it.
4- Dwell- I've tried between 4.5 - 5.5ms running, no difference. (stock igniter and coils)
5- Plugs: Tried BKR7E at .035" and IFR8H at .028" with no difference. Again, a genuine misfire wouldn't affect the tach. I guess I can re-gap my 7Es to .02" before I re-install 'em.
6- Abe, I just nixed the capacitors, and will retry after I get HR code re-loaded.
#11
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Update: I started drinking with a very nice Barleywine Ale at about 4pm when I gave up for the day (just after you called me.) I continued drinking until I became drunk (there was some Porter, and then a couple IPAs), and then I drank some more. We're on Rum & Coke at the moment.
During this time I have removed the MS, desoldered the capacitors from the comparator circuit, resoldered the five other wires that accidentally popped off when I did that (hopefully in the same places). I then came inside and started going through my MSQ one screen at a time, making various adjustments like raising the overboost limit, going back to earlier, more conservative fuel and ignition maps (just in case) and making a few other tweaks that I've already forgotten but must have seemed logical at the time.
In other words, it will be a miracle if the car starts tomorrow morning.
If it does, we still on for around noon? That beer ain't gonna bottle itself, and I'm dying to taste how it came out. You guys already racked it into the secondary, right?
During this time I have removed the MS, desoldered the capacitors from the comparator circuit, resoldered the five other wires that accidentally popped off when I did that (hopefully in the same places). I then came inside and started going through my MSQ one screen at a time, making various adjustments like raising the overboost limit, going back to earlier, more conservative fuel and ignition maps (just in case) and making a few other tweaks that I've already forgotten but must have seemed logical at the time.
In other words, it will be a miracle if the car starts tomorrow morning.
If it does, we still on for around noon? That beer ain't gonna bottle itself, and I'm dying to taste how it came out. You guys already racked it into the secondary, right?
#14
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Yeah, sorry. I was debating which one to post, over the past few days I've been blowing through a lot of 'em.
Here's an example from the 11'th. This was after I built the opto-based second trigger circuit, I was running HR10f at the time. If you're wondering why the Spark1 table looks so strange, this one has map-switching enabled for the spark- this is a safety feature. When the WI system turns on, the pressure in the line switches the system to Spark2 which is more aggressive in boost.
The RPM spike at 461.5 is pretty obvious. There's another at 926.4, another at 1106.5, and some little ones from ~760 - 801.
I've done so many test drives the past few days I can't remember exactly where each tachometer dropout / misfire occurred. I ought to hook a button up to one of the inputs so I can hit it to insert a marker in the log every time something odd happens.
Here's an example from the 11'th. This was after I built the opto-based second trigger circuit, I was running HR10f at the time. If you're wondering why the Spark1 table looks so strange, this one has map-switching enabled for the spark- this is a safety feature. When the WI system turns on, the pressure in the line switches the system to Spark2 which is more aggressive in boost.
The RPM spike at 461.5 is pretty obvious. There's another at 926.4, another at 1106.5, and some little ones from ~760 - 801.
I've done so many test drives the past few days I can't remember exactly where each tachometer dropout / misfire occurred. I ought to hook a button up to one of the inputs so I can hit it to insert a marker in the log every time something odd happens.
#15
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I used to get those spikes, and Mr. Hoffman advised that grounds needed to be beefed up. He was correct. We ended up running a couple more 18 (or was it 16?) gauge grounds from the MS' board to the back of the cylinder head. Fixed 'er up.
#17
Another member of the "slight misfire sometimes" club. I usually have a misfire to 0 RPMs on datalogs every 15minutes. I have found one thing oddly strange though. I can push a particular button on my car and the problem goes away. If I run the A/C, it will never misfire. Weirdest thing ever. Have no clue why and how but I guarantee it will occasionally misfire about every 15 minutes, but NEVER with A/C on.
#18
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No, I managed to snag a bottle of Stone Old Guardian a few weeks ago, and today seemed like the right time to crack it open. And now that I think about it, their 2008 Imperial Stout was just released- I need to get off my *** and track some down pronto!
But the one I'd really like to find, and call me ******* crazy, is an Oskar Blues Old Chub. A few years ago I was in Denver just after the big annual huzzah, and on the way to the airport I dropped by to see a friend who lives there. He took me to a place called the Falling Rock, where they had about two gallons left from the competition of what may be the most divine oak-casked Scottish Strong Ale I have ever consumed. It was one of OB's entries that year, and from what I can piece together it was essentially just off-the-shelf Old Chub that they aged for 18 months in a whiskey cask. Granted, I'll never experiance that particular beer again, but I'd like to at least see what their "regular" stuff is like.
Already done as part of the original install.
But the one I'd really like to find, and call me ******* crazy, is an Oskar Blues Old Chub. A few years ago I was in Denver just after the big annual huzzah, and on the way to the airport I dropped by to see a friend who lives there. He took me to a place called the Falling Rock, where they had about two gallons left from the competition of what may be the most divine oak-casked Scottish Strong Ale I have ever consumed. It was one of OB's entries that year, and from what I can piece together it was essentially just off-the-shelf Old Chub that they aged for 18 months in a whiskey cask. Granted, I'll never experiance that particular beer again, but I'd like to at least see what their "regular" stuff is like.
Originally Posted by Ben
We ended up running a couple more 18 (or was it 16?) gauge grounds from the MS' board to the back of the cylinder head. Fixed 'er up.
#19
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Yeah, you'd think that, but the MS works in mysterious ways. My car had the same issue (high-load misfires), and the tach would drop away (sometimes all the way to 0). Gapped the BKR7Es to .024 and the misfires are gone.
#20
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Update:
The coffee stout spent a total of three weeks in the primary and a week and a half in the secondary. Yesterday afternoon we bottled. Due to the fact that we failed to properly inspect the bottles prior to sanitizing them, we ended up with a large number of sanitized yet very yucky bottles, which fortunately we caught and set aside during the filling process. As a result, we ran out after 39 bottles and put the remainder into a 2 liter growler.
I forget what the final gravity was- Abe wrote it down, but I recall that it worked out to just over 5% expected ABV. We tasted the sample from the hydrometer tube, and despite what might have been called "questionable" sanitizing procedures during the initial brew (Abe, you have to *wash* your hands, with soap, to get all the Miata grease off before you dunk them in the solution) it was wonderful. Just a few more weeks to go as our beautiful little yeast perform their final duty.
Guess I should give an update on the car too...
Yesterday was much improved. I got the misfire only twice (out of a 50+ mile round trip).
Unfortunately, I changed about ten different things, and so I don't know what the fix was. I am hoping that it was the somewhat different cap values that I installed in the CMP/CKP pickup filter. I finally got off my *** and breadboarded that part of the circuit so I can swap values at will. There's something amazingly geeky about driving around with a protoboard taped to the floor of your car next to the case-less ECU with wires criss-crossing between the two. I'm going to try some different values this afternoon at lunch time, and see whether moving lower or higher makes a difference.
It still astounds me that people aren't screaming like hell about this sort of problem. I can't believe that every single one of you either hasn't experienced it, or was content to just fiddle around with random capacitors until it worked right.
Gonna be out of town tomorrow and Wednesday, so that leaves only today, and Thursday through Saturday to get this all figured out and put back into soldered form before the big run on Sunday. The dyno trip will have to wait- I'll be happy if my ECU is fully re-assembled in time. Guess I'll just have to turn down the boost a bit and run towards the rear of the pack...
The coffee stout spent a total of three weeks in the primary and a week and a half in the secondary. Yesterday afternoon we bottled. Due to the fact that we failed to properly inspect the bottles prior to sanitizing them, we ended up with a large number of sanitized yet very yucky bottles, which fortunately we caught and set aside during the filling process. As a result, we ran out after 39 bottles and put the remainder into a 2 liter growler.
I forget what the final gravity was- Abe wrote it down, but I recall that it worked out to just over 5% expected ABV. We tasted the sample from the hydrometer tube, and despite what might have been called "questionable" sanitizing procedures during the initial brew (Abe, you have to *wash* your hands, with soap, to get all the Miata grease off before you dunk them in the solution) it was wonderful. Just a few more weeks to go as our beautiful little yeast perform their final duty.
Guess I should give an update on the car too...
Yesterday was much improved. I got the misfire only twice (out of a 50+ mile round trip).
Unfortunately, I changed about ten different things, and so I don't know what the fix was. I am hoping that it was the somewhat different cap values that I installed in the CMP/CKP pickup filter. I finally got off my *** and breadboarded that part of the circuit so I can swap values at will. There's something amazingly geeky about driving around with a protoboard taped to the floor of your car next to the case-less ECU with wires criss-crossing between the two. I'm going to try some different values this afternoon at lunch time, and see whether moving lower or higher makes a difference.
It still astounds me that people aren't screaming like hell about this sort of problem. I can't believe that every single one of you either hasn't experienced it, or was content to just fiddle around with random capacitors until it worked right.
Gonna be out of town tomorrow and Wednesday, so that leaves only today, and Thursday through Saturday to get this all figured out and put back into soldered form before the big run on Sunday. The dyno trip will have to wait- I'll be happy if my ECU is fully re-assembled in time. Guess I'll just have to turn down the boost a bit and run towards the rear of the pack...