The new transmission seems to be decent but now there’s a new problem. The motor started filling my catch cans with oil, both cans full, after only a few laps. Lots of smoke on hard acceleration and deceleration out the exhaust. Did a compression test and cylinder 1 is way down, leak down cylinder one lost like 80%.
So time to pull the motor. https://i.imgur.com/cJCc6WT.jpg https://i.imgur.com/WeGn7Zk.jpg https://i.imgur.com/KmeNKf4.jpg https://i.imgur.com/3u7VN6K.jpg https://i.imgur.com/bP9yPF0.jpg Found the problem https://i.imgur.com/aw0cx0y.jpg https://i.imgur.com/0h8Hy9y.jpg https://i.imgur.com/7uxsKJH.jpg 8 hard years on that motor, piston finally let go. Picked up a junkyard 1997 motor, hoping it’s usable. https://i.imgur.com/nOHNyc7.jpg |
Bummer, but congrats for getting it to live this long.
|
Junk yard motor swap continued...
Leak down test, air leaking out of the exhaust and intake manifold, decided to swap my head on. At least this would save some time dealing with injectors and other stuff. https://i.imgur.com/7IwPUHu.jpg Cleaned up my head. https://i.imgur.com/jXGzCKC.jpg Swapping the head was a bit of a last minute call, couldn't find a Mazda head gasket on such short notice, so went with a felpro. Reused the ARP headstuds. https://i.imgur.com/QSF2p86l.jpg https://i.imgur.com/QRX0a2nl.jpg https://i.imgur.com/CWMN1Ztl.jpg Parts from moss https://i.imgur.com/TrismeKl.jpg Swapped my pan on, this build is sponsored by Felpro https://i.imgur.com/taRA2zol.jpg https://i.imgur.com/KcAIKhOl.jpg https://i.imgur.com/QCnqBVGl.jpg Looking like a motor again https://i.imgur.com/vFep281l.jpg https://i.imgur.com/EC0Ipzdl.jpg I cracked a coolant hardline for the turbo when shuffling around the head. https://i.imgur.com/FmjpAgsl.jpg Placed an order with FlyinMiata https://i.imgur.com/A8WJN7Jl.jpg https://i.imgur.com/kO69HQYl.jpg Motor in the car https://i.imgur.com/QlnzmGwl.jpg Test drive... https://i.imgur.com/39pFnoxl.jpg https://i.imgur.com/6A5KxZ3l.jpg |
Holy crap! Nice rebound and quick work on the wrenching so that you could get back to driving. This is how it's done. Goood shit and the new motor sounds nice and healthy.
I might have missed this, do you run this thing on pump or e85? I'm certain it's in this thread somewhere, just curious. Haven't seen too many ringland failures so I'm kinda of surprised (but not really seeing how much abuse it has seen). Just curious if detonation might have been a factor or if it just let go. |
Originally Posted by Fireindc;[url=tel:1639945
1639945[/url]]Holy crap! Nice rebound and quick work on the wrenching so that you could get back to driving. This is how it's done. Goood shit and the new motor sounds nice and healthy.
I might have missed this, do you run this thing on pump or e85? I'm certain it's in this thread somewhere, just curious. Haven't seen too many ringland failures so I'm kinda of surprised (but not really seeing how much abuse it has seen). Just curious if detonation might have been a factor or if it just let go. |
Drove at GridLife Circuit Legends at Lime Rock Park. Awesome track and event.
|
The junkyard motor continues to do it's thing.
Three camera angles, same run. |
All times are GMT -4. The time now is 12:16 PM. |
© 2024 MH Sub I, LLC dba Internet Brands