MEGAsquirt A place to collectively sort out this megasquirt gizmo

Seemingly random boost cut 1.6t ms2pnp

Thread Tools
 
Search this Thread
 
Old 06-05-2020, 11:07 PM
  #1  
Newb
Thread Starter
 
drakec9's Avatar
 
Join Date: Nov 2019
Location: Charlotte, NC
Posts: 35
Total Cats: 2
Default Seemingly random boost cut 1.6t ms2pnp

Hello all, I have been learning to tune megasquirt myself for awhile now, i installed an ms2pnp long before my turbo build to learn the ins and outs before putting my engine at risk with boost and no knowledge. I have since installed by turbo with all the supporting mods necessary and have began the journey of tuning my first turbo miata. Im in a 92 1.6L with a gt2554r, walbro 255 pump, flowforce 640cc injectors, turbosmart manual boost controller(turned all the way down) and turbosmart bov, intercooled setup running 7-9psi. The boost hits early most ive ever seen is 8.8psi and tapers down to 7.5psi or so as the rpm rises. While i have only been at this for a few days, i have ran into a couple of issues along the way. I have tuned only fuel so far for idle the way i want it, low rpm, some of cruise and i have been working on high rpm and load. i have accel enrichment off and timing fixed (not 'use table') and the fuel calculation does no include afr target table. The biggest problem i am battling right now is what seems to be a random, but probably isnt, boost cut. The first occurrence surprised me a bit but shouldnt have because i failed to replace my spark plugs before i started this process. I changed them to NGK heat range 7 plugs gaped at .30. The second occurrence really surprised me, 1st gear, WOT felt like i hit redline early, i did catch this one on a datalog which i will provide, i am not very good at reading datalogs, i cannot find any issue with anything except for imperfect afrs, range from 11.5-12.5 but a little inconsistent (still working on fuel table). The next time i experienced this boost cut was a few minutes ago on the way to pick up dinner. This time i was in 4th gear, close to WOT and seemed to be lower in rpm range around 4500-5500 but i was looking at the wideband and boost gauge not the tachometer. I also was not data logging because im stupid. i suspect this may be due to a too rich air fuel mixture i notice that sometimes i was getting down to he 10s in boost. I honestly do not know any other cause for boost cut other than spark blowing out or terrible afrs. I know my tune in probably terrible i am still learning and i have never driven a turbo car before so i did interpolate some on the fuel table and hit some boost. i probably jumped the gun and skipped some things but i do not want to damaged anything and i know hitting boost cut is not good for anything especially my engine and engine mounts. i have replaced every seal and gasket as well as the timing belt and water pump (twice now) i do not suspect this is a mechanical problem. My next step will be to check the base timing again and also pull the new plugs out and check them. Is there anything i am missing or any tips some of you gurus have for me to solve this boost cut? i will provide my tune and datalog mentioned above any input is greatly appreciated and criticism is welcome as long as it is constructive, i am trying to learn a much as i can.
Attached Files
File Type: mlg
2020-06-04_20.53.45.mlg (795.2 KB, 21 views)
File Type: msq
CurrentTune.msq (117.5 KB, 21 views)
drakec9 is offline  
Old 06-05-2020, 11:17 PM
  #2  
Newb
Thread Starter
 
drakec9's Avatar
 
Join Date: Nov 2019
Location: Charlotte, NC
Posts: 35
Total Cats: 2
Default

boost cut occured at 1549 of 4194 on the datalog
drakec9 is offline  
Old 06-06-2020, 12:28 PM
  #3  
Senior Member
 
SpartanSV's Avatar
 
Join Date: Apr 2017
Location: Greeley, CO
Posts: 1,226
Total Cats: 169
Default

Originally Posted by drakec9
boost cut occured at 1549 of 4194 on the datalog
You hit 150 kpa at that point. Your boost cut setting is 150 kpa. It's doing exactly what you're telling it to do.
SpartanSV is offline  
Old 06-06-2020, 05:26 PM
  #4  
Newb
Thread Starter
 
drakec9's Avatar
 
Join Date: Nov 2019
Location: Charlotte, NC
Posts: 35
Total Cats: 2
Default

Oh jeez, I never even knew that was there thank you the help spartan I feel kind of stupid but at least the problem is fixed
drakec9 is offline  
Related Topics
Thread
Thread Starter
Forum
Replies
Last Post
Spei
DIY Turbo Discussion
6
02-23-2020 02:08 AM
NASSEX
Engine Performance
21
06-21-2019 10:34 PM
HeresJohnny
MEGAsquirt
45
02-20-2014 04:20 AM
devin mac
MEGAsquirt
2
05-13-2008 07:19 PM
Ajb
General Miata Chat
3
03-30-2008 07:32 AM



Quick Reply: Seemingly random boost cut 1.6t ms2pnp



All times are GMT -4. The time now is 11:30 PM.