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Turbo Blowing White Smoke?

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Old Sep 18, 2014 | 01:40 PM
  #21  
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Im going to try and use gasoline and brake clean to clean all that out. Is this normal when a turbo seal gives to leak THAT much oil?

on a side note 18psi, i called usps to give me an update on tracking info, since that number hasnt been updated all week. theyre saying i should see it monday

At anyrate shouldnt be long until the cars back on the road!
Old Sep 18, 2014 | 01:49 PM
  #22  
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I've no idea, apparently it completely burst open? that's a ton of oil.
gasoline and degreaser would be what I'd use. or maybe just degreaser, like purple power or something.

I've pretty much had terrible experience with every carrier lately. USPS, Fedex, all are idiots. I just pack really really well, and insure for at least the total amount, and hope for the best.
Old Sep 18, 2014 | 01:57 PM
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Holy wow. Nice find.. have fun with the new turbo.
Old Sep 18, 2014 | 02:07 PM
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No worries man it is what is. Theres still other stuff i can do to clean up the car in the mean time. If im able to get the car back together and around 250whp before snowfall this year ill be happy!
Old Sep 18, 2014 | 02:24 PM
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That's incredible! Top marks, great failure!
Old Sep 20, 2014 | 08:15 AM
  #26  
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Yes! My turbo came in late yesterday, maybe today or tomorrow I'll get around to installing it
Attached Thumbnails Turbo Blowing White Smoke?-img_20140919_180546_zpsftspnwqh.jpg   Turbo Blowing White Smoke?-img_20140919_180612_zpsposj3ply.jpg  

Last edited by shredheads666; Sep 20, 2014 at 01:15 PM.
Old Sep 20, 2014 | 01:17 PM
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that box looks like it got gangbanged by elephants.
way to go usps.
glad I packed the heck out of it.
Old Sep 20, 2014 | 01:21 PM
  #28  
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They saw the word fragile on it and thought orly!?
Old Sep 20, 2014 | 11:20 PM
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Oh it must be french they thought
Old Sep 22, 2014 | 04:37 PM
  #30  
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Almost got it installed over the weekend. Just need to bolt on the down pipe and reroute bottom coolant hose ,intercooler piping is now in the way

NA/NB Compatibility Guide

I'm thinking i can use the lower coolant hose from a NB? but im open to suggestions
Old Sep 27, 2014 | 06:39 PM
  #31  
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New turbo spits oil and I don't know why? -4 an to a restrictor. Then -10 an as a return. Maybe the line could get b straightend out better.



Also when throttle is applied the car the motor stalls?
I replaced the throttle body because my brother and I heard an electrical hum from the idle air control valve.
But the car still stalls out



Homer might be right at this point

Any suggestions why the motor would stall?
Attached Thumbnails Turbo Blowing White Smoke?-img_20140927_180513_zpsr6b3k2c2.jpg   Turbo Blowing White Smoke?-http3a2f2f31.media.tumblr.com2f6ecd2a8e793a78b26670d51385a83c632ftumblr_nccdy4ialh1rldpfao1_500_.jpg  
Old Sep 27, 2014 | 06:41 PM
  #32  
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Maybe an engine bay picture would help?
Attached Thumbnails Turbo Blowing White Smoke?-img_20140927_180549_zpsclc1rczn.jpg  
Old Sep 27, 2014 | 08:02 PM
  #33  
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how straight is the oil return?

and did you make sure all the bolts/fasteners were torqued to spec per my note?
Old Sep 28, 2014 | 11:57 AM
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Check that oil return. 2 turbos spitting oil makes it sound like a blockage in the return to me.
Old Sep 28, 2014 | 10:46 PM
  #35  
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I'm going to redo that line and see if that helps.

18 psi yeah i tightened everything down, and the turbo was clocked the correct way you shipped it too!

Anyone have the same problem with the motor stalling? When i searched it, the problem was solved once the valve was replaced. It has to be something dumb because the car was running pretty good until the turbo seals went bad spit all that oil into my intercooler
Old Sep 29, 2014 | 11:26 AM
  #36  
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Those two breather lines going to the same little can inlet are too small and you are possibly building backpressure in the crankcase.

High crankcase pressure can push oil out of seals.

Last edited by sixshooter; Sep 29, 2014 at 12:18 PM.
Old Sep 29, 2014 | 01:14 PM
  #37  
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I deffinitly have high crank case pressure, i noticed that the other day too. ill redo those lines and let you guys know what happens. Thanks for the heads up!
Old Oct 12, 2014 | 08:11 PM
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Any updates? Curious what the problem turns out to be
Old Oct 13, 2014 | 11:50 AM
  #39  
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No idea, im at the point of tearing it down and seeing if i possibly cracked a piston from the dyno pulls? But im fed up with the car and low on cash so itll probably sit broken until spring. if anything changes ill update the thread. thanks to everyone helping me troubleshoot it!
Old Oct 14, 2014 | 12:59 AM
  #40  
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My white smoke was from blown rings. Leak down was actually OK too. Shoulda run compression too...



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