T3 60 trim, dyno 2 at 22 psi
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22psi and 225whp? seriously?
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Originally Posted by 18psi
(Post 891104)
22psi and 225whp? seriously?
So do I |
I made those numbers with like 14psi on a 2554. Something is way off with your setup.
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well let me know what it maybe I'll be more then happy to fix it
at 22psi it was dropping out of boost down to 16 psi up top |
Dude. I was so excited to see that someone else was running man boost.
But then I saw the world's saddest dyno chart. Your boost taper is prolly due to VE fail. Still though. Even with 16psi you should be at well over 200hp. Please provide your build list of everything. I got the first item: Zipties. |
I think around 12 psi it was at 180 whp at higher rpm, I'll have to check again
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Here is a comparsion of 20psi taper to 16 with some knock at the end of the run vs 12psi hold
https://www.miataturbo.net/attachmen...ine=1339954369 adult image hosting |
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this was mine at 13psi:
https://www.miataturbo.net/attachmen...ine=1339955978 why are you choking up so much up top? that turbine flows much better than a gt28 and the compressor is good for ~300rwhp |
I"m not sure, I"m gonna retry later and remove the exhaust and just run the downpipe down and see if it holds boost out to the end of the revs
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If I remember your build thread (that I unsubscribed from because I was disgusted) correctly then this dyno plot really doesn't surprise me. Heck, I'm impressed the car is running at all, actually.
But can you post up a full list of your setup? |
t3 60 trim off a nissan vg30e using a .48 ar turbine housing
2.5in all the way back to a flowtech warlock muffler exhaust tacotaco turbo log header evo 8 intercooler stock coils with platnium plugs gapped down to .034 ngk 6 heat range ebay xtd clutch 6 puck - slipping rx7 460cc injectors fuel held steady around 12 to 11 range. Knock was occuring at high rpm range, 6200-7000. 93 AKI only, no screwing around. |
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onset of a 35r with power of a 2554.
umm, yeah. Perhaps its the slipping clutch, I dont know |
learning process.
Just some issues here and there to fix. |
Originally Posted by 18psi
(Post 891400)
onset of a 35r with power of a 2554.
umm, yeah. Perhaps its the slipping clutch, I dont know the pulls posted were 3rd gear pulls due to slipping clutch in 4th gear. But you can see it pushed power production farther back, really nothing to be susprised about. Also since I went testing on my car, I puilled the exhaust off and left the downpipe on it. I went from 80% duty cycle to 95% duty cycle. Still same boost drop out issue. Next plan is to make a dual port wastegate using the current wastegate. |
or perhaps you never mentioned load at all and we all were led to believe that like a NORMAL person, you started the pull in the 1:1 gear at 2k
even ignoring the shape of the curve, those numbers are pathetic |
Originally Posted by 18psi
(Post 891409)
or perhaps you never mentioned load at all and we all were led to believe that like a NORMAL person, you started the pull in the 1:1 gear at 2k
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God damn someone please ban this person.
I think I feel such loathing because he reminds me of myself. |
Originally Posted by Braineack
(Post 891142)
this was mine at 13psi:
https://www.miataturbo.net/attachmen...ine=1339955978 why are you choking up so much up top? that turbine flows much better than a gt28 and the compressor is good for ~300rwhp |
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