Andy Hollis' One Lap Miata (K24 Honda power)
#261
...and it's done.
Lots of hours, lots of creativity. Apex Auto Works really knocked it out of the park.
Those are 255/40-17 Dunlops on 10" wide XXR's. We'll be doing the five-lug conversion next week so we can mount the 255/35-18 RE71's on 18x10.5 ET15 RPF1's...and later the 285/30-18 when available in March.
I'm at Daytona for the Rolex 24 where we are displaying the car at the GRM tent.
You can see more pics by going to the One Lap Miata FB page and also Apex Auto Works. I'll post under the cover shots as I get bandwidth.
Lots of hours, lots of creativity. Apex Auto Works really knocked it out of the park.
Those are 255/40-17 Dunlops on 10" wide XXR's. We'll be doing the five-lug conversion next week so we can mount the 255/35-18 RE71's on 18x10.5 ET15 RPF1's...and later the 285/30-18 when available in March.
I'm at Daytona for the Rolex 24 where we are displaying the car at the GRM tent.
You can see more pics by going to the One Lap Miata FB page and also Apex Auto Works. I'll post under the cover shots as I get bandwidth.
#272
Man, the work those guys did on those tubbed fenders is beyond belief. I'm not sure I've ever seen that done that well before. The wheel choice 100% makes sense for your use of the car. When I first saw that you were doing it, I kinda thought the car would look silly, but honestly it looks really good.
Can't wait to see you take on the OLOA group with this thing.
Can't wait to see you take on the OLOA group with this thing.
#274
Those of you following on FB have seen a hint of this, but I'm finally pulling the motor to investigate.
This is my "good" motor. A pro-built sleeved shortblock, with CNC-ported head...and my usual cams and such. Manley rods with ARP bolts. Made about 300hp to the wheels in my CRX. Low hours, never money-shifted. Happened at COTA in T7 after a 4-3 downshift ending up at about 7000rpm. Rev limiter had been reduced from the usual 8500 to 8200 for the day to reduce stress on the motor. Fresh oil change with Redline 30w Racing. Datalogs look normal, save the knock sensor spikes when the things came apart.
I de-clutched immediately when I felt it go, and it appears to have stopped rotations quickly. Fingers crossed that the head is undamaged.
Pulling the motor now...here's the first pics...
This is my "good" motor. A pro-built sleeved shortblock, with CNC-ported head...and my usual cams and such. Manley rods with ARP bolts. Made about 300hp to the wheels in my CRX. Low hours, never money-shifted. Happened at COTA in T7 after a 4-3 downshift ending up at about 7000rpm. Rev limiter had been reduced from the usual 8500 to 8200 for the day to reduce stress on the motor. Fresh oil change with Redline 30w Racing. Datalogs look normal, save the knock sensor spikes when the things came apart.
I de-clutched immediately when I felt it go, and it appears to have stopped rotations quickly. Fingers crossed that the head is undamaged.
Pulling the motor now...here's the first pics...
#275
As you can see, the rod bolts are broken. First time I've seen that in any of my K builds/failures.
At this point, I am putting the original spare stock TSX motor back in until I get to the bottom of the issue at hand.
I've also spent some time over the last two weeks setting up Plan B...killer deal on something special fell into my lap. Something VERY special.
PS: I have a complete spare pro-built sleeved shortblock, and another CNC'd head on the shelf. But none of that is going in the car until I am confident that I have identified the weak point and fixed it.
At this point, I am putting the original spare stock TSX motor back in until I get to the bottom of the issue at hand.
I've also spent some time over the last two weeks setting up Plan B...killer deal on something special fell into my lap. Something VERY special.
PS: I have a complete spare pro-built sleeved shortblock, and another CNC'd head on the shelf. But none of that is going in the car until I am confident that I have identified the weak point and fixed it.