General Miata Chat A place to talk about anything Miata

i might have blown my turbo

Thread Tools
 
Search this Thread
 
Old 02-09-2008, 07:06 PM
  #1  
I'm Miserable!
Thread Starter
iTrader: (5)
 
bryantaylor's Avatar
 
Join Date: Dec 2006
Location: jacksonville, fl
Posts: 1,711
Total Cats: -1
Default i might have blown my turbo

i have a DSM 13g. i did a little work on the intercooler pipes today and put my boost controller back on set to 14psi. first pull ok, it spooled up and held boost for a few seconds, but now it just doesnt want to spool up. and it only will make like 2-3psi in 1st gear. it will get to 9psi at most, but takes forever, and you cant really hear it spool like it did before. i might have some boost leaks, but i should still be able to hear the turbo spool up. no smoke that i can see. i even swaped a different BOV over, and it had no change. i will try and mess with the charge pipes some tomorow, but everything seems to look ok.
bryantaylor is offline  
Old 02-09-2008, 07:26 PM
  #2  
I'm Miserable!
Thread Starter
iTrader: (5)
 
bryantaylor's Avatar
 
Join Date: Dec 2006
Location: jacksonville, fl
Posts: 1,711
Total Cats: -1
Default

i might just say screw it and get one of these
http://cgi.ebay.com/ebaymotors/T3-T4...spagenameZWDVW
bryantaylor is offline  
Old 02-09-2008, 07:34 PM
  #3  
Elite Member
iTrader: (2)
 
mazda/nissan's Avatar
 
Join Date: Jan 2007
Location: Lexington, SC
Posts: 2,075
Total Cats: 0
Default

what about your megan manifold?
mazda/nissan is offline  
Old 02-09-2008, 07:47 PM
  #4  
Boost Czar
iTrader: (62)
 
Braineack's Avatar
 
Join Date: May 2005
Location: Chantilly, VA
Posts: 79,494
Total Cats: 4,080
Default

only a few ways a turbo can fail. the blades are rubbing against the walls, it has no blades or the oil "seals" leak oil.

sounds liek you simply have an exhaust or boost leak. bet you lost a coupler, happen to almost everyone you finally breaches 10psi.
Braineack is offline  
Old 02-09-2008, 08:04 PM
  #5  
I'm Miserable!
Thread Starter
iTrader: (5)
 
bryantaylor's Avatar
 
Join Date: Dec 2006
Location: jacksonville, fl
Posts: 1,711
Total Cats: -1
Default

all the couplers are still there. mani is fine, you can hear it when it was cracked.
bryantaylor is offline  
Old 02-09-2008, 08:23 PM
  #6  
:(
iTrader: (7)
 
magnamx-5's Avatar
 
Join Date: Jul 2006
Location: nowhere
Posts: 8,255
Total Cats: 4
Default

dude i had the same trouble on my 16g turned out to be a leak on my compressor from where i clocked the turbo.
magnamx-5 is offline  
Old 02-09-2008, 08:24 PM
  #7  
I'm Miserable!
Thread Starter
iTrader: (5)
 
bryantaylor's Avatar
 
Join Date: Dec 2006
Location: jacksonville, fl
Posts: 1,711
Total Cats: -1
Default

Originally Posted by magnamx-5
dude i had the same trouble on my 16g turned out to be a leak on my compressor from where i clocked the turbo.
i will check that, but i never even touched the turbo really today.
bryantaylor is offline  
Old 02-09-2008, 09:00 PM
  #8  
Elite Member
iTrader: (5)
 
m2cupcar's Avatar
 
Join Date: Jan 2005
Location: Atlanta
Posts: 7,486
Total Cats: 372
Default

Originally Posted by bryantaylor
...i did a little work on the intercooler pipes today....
Take apart or reinstall couplers/clamps? I vote boost leak.
m2cupcar is offline  
Old 02-09-2008, 09:08 PM
  #9  
I'm Miserable!
Thread Starter
iTrader: (5)
 
bryantaylor's Avatar
 
Join Date: Dec 2006
Location: jacksonville, fl
Posts: 1,711
Total Cats: -1
Default

it was fine the first time i boosted, it turned to **** while i was driving. i will triple check the pipes again tomorow
bryantaylor is offline  
Old 02-09-2008, 09:36 PM
  #10  
:(
iTrader: (7)
 
magnamx-5's Avatar
 
Join Date: Jul 2006
Location: nowhere
Posts: 8,255
Total Cats: 4
Default

If it was fine until you hit boost for abit something is leaking. You can
A presurize the system to leak test it
B take apart and reinstall all the components
C give up and drive a slow NA
Two of these options should appeal to you GL.
magnamx-5 is offline  
Old 02-09-2008, 11:04 PM
  #11  
Elite Member
iTrader: (5)
 
m2cupcar's Avatar
 
Join Date: Jan 2005
Location: Atlanta
Posts: 7,486
Total Cats: 372
Default

I agree - taking apart and reassembling was what fixed my mystery leak
m2cupcar is offline  
Old 02-09-2008, 11:15 PM
  #12  
I'm Miserable!
Thread Starter
iTrader: (5)
 
bryantaylor's Avatar
 
Join Date: Dec 2006
Location: jacksonville, fl
Posts: 1,711
Total Cats: -1
Default

i have done it once already, but i will try again. but i am kinda dreaming of a t3/t4 now, lol. i wonder how bad the spool up time will be?
bryantaylor is offline  
Old 02-10-2008, 12:09 AM
  #13  
Elite Member
iTrader: (9)
 
miatamania's Avatar
 
Join Date: Aug 2006
Location: Concord, North Carolina
Posts: 4,160
Total Cats: 6
Default

that would depend on the size...

I've vote a leak somewhere.
miatamania is offline  
Old 02-10-2008, 10:09 AM
  #14  
Elite Member
iTrader: (5)
 
m2cupcar's Avatar
 
Join Date: Jan 2005
Location: Atlanta
Posts: 7,486
Total Cats: 372
Default

I think somebody posted 10psi at 4200rpm - but there's a LOT of deciding factors on spool, including the actual components of the t3/t4 (as mentioned). That would be too much turbo for a small engine IMO.
m2cupcar is offline  
Old 02-10-2008, 12:04 PM
  #15  
Elite Member
iTrader: (21)
 
paul's Avatar
 
Join Date: Jun 2006
Location: Point Pleasant, NJ
Posts: 2,957
Total Cats: 2
Default

Originally Posted by bryantaylor
i have done it once already, but i will try again. but i am kinda dreaming of a t3/t4 now, lol. i wonder how bad the spool up time will be?

i bet the spool will be better than what you are dealing with now

Originally Posted by bryantaylor
it will get to 9psi at most, but takes forever,
paul is offline  
Old 02-10-2008, 02:17 PM
  #16  
I'm Miserable!
Thread Starter
iTrader: (5)
 
bryantaylor's Avatar
 
Join Date: Dec 2006
Location: jacksonville, fl
Posts: 1,711
Total Cats: -1
Default

LOL, thanks paul
bryantaylor is offline  
Old 02-11-2008, 07:31 PM
  #17  
I'm Miserable!
Thread Starter
iTrader: (5)
 
bryantaylor's Avatar
 
Join Date: Dec 2006
Location: jacksonville, fl
Posts: 1,711
Total Cats: -1
Default

well sports fans, it was a hairline crack in the mani. but it was so small, i couldnt feel any air coming out while at idle. but as soon as i touched it with the welder, it burned right through. it all back together and boosting now, woot!
bryantaylor is offline  
Old 02-11-2008, 10:30 PM
  #18  
Elite Member
iTrader: (2)
 
mazda/nissan's Avatar
 
Join Date: Jan 2007
Location: Lexington, SC
Posts: 2,075
Total Cats: 0
Default

Originally Posted by mazda/nissan
what about your megan manifold?
100 PTS.!!!
mazda/nissan is offline  
Related Topics
Thread
Thread Starter
Forum
Replies
Last Post
Full_Tilt_Boogie
Build Threads
84
04-12-2021 04:21 PM
Rick02R
WTB
3
01-03-2016 07:18 PM
tazswing
Race Prep
20
10-03-2015 11:04 AM
cale saurage
DIY Turbo Discussion
16
10-01-2015 11:25 AM



Quick Reply: i might have blown my turbo



All times are GMT -4. The time now is 09:48 PM.