Drift car from MA
#301
The new transmission seems to be decent but now there’s a new problem. The motor started filling my catch cans with oil, both cans full, after only a few laps. Lots of smoke on hard acceleration and deceleration out the exhaust. Did a compression test and cylinder 1 is way down, leak down cylinder one lost like 80%.
So time to pull the motor.
Found the problem
8 hard years on that motor, piston finally let go.
Picked up a junkyard 1997 motor, hoping it’s usable.
So time to pull the motor.
Found the problem
8 hard years on that motor, piston finally let go.
Picked up a junkyard 1997 motor, hoping it’s usable.
#303
Junk yard motor swap continued...
Leak down test, air leaking out of the exhaust and intake manifold, decided to swap my head on. At least this would save some time dealing with injectors and other stuff.
Cleaned up my head.
Swapping the head was a bit of a last minute call, couldn't find a Mazda head gasket on such short notice, so went with a felpro. Reused the ARP headstuds.
Parts from moss
Swapped my pan on, this build is sponsored by Felpro
Looking like a motor again
I cracked a coolant hardline for the turbo when shuffling around the head.
Placed an order with FlyinMiata
Motor in the car
Test drive...
Leak down test, air leaking out of the exhaust and intake manifold, decided to swap my head on. At least this would save some time dealing with injectors and other stuff.
Cleaned up my head.
Swapping the head was a bit of a last minute call, couldn't find a Mazda head gasket on such short notice, so went with a felpro. Reused the ARP headstuds.
Parts from moss
Swapped my pan on, this build is sponsored by Felpro
Looking like a motor again
I cracked a coolant hardline for the turbo when shuffling around the head.
Placed an order with FlyinMiata
Motor in the car
Test drive...
#304
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Holy crap! Nice rebound and quick work on the wrenching so that you could get back to driving. This is how it's done. Goood **** and the new motor sounds nice and healthy.
I might have missed this, do you run this thing on pump or e85? I'm certain it's in this thread somewhere, just curious. Haven't seen too many ringland failures so I'm kinda of surprised (but not really seeing how much abuse it has seen). Just curious if detonation might have been a factor or if it just let go.
I might have missed this, do you run this thing on pump or e85? I'm certain it's in this thread somewhere, just curious. Haven't seen too many ringland failures so I'm kinda of surprised (but not really seeing how much abuse it has seen). Just curious if detonation might have been a factor or if it just let go.
#305
Originally Posted by Fireindc;[url=tel:1639945
1639945[/url]]Holy crap! Nice rebound and quick work on the wrenching so that you could get back to driving. This is how it's done. Goood **** and the new motor sounds nice and healthy.
I might have missed this, do you run this thing on pump or e85? I'm certain it's in this thread somewhere, just curious. Haven't seen too many ringland failures so I'm kinda of surprised (but not really seeing how much abuse it has seen). Just curious if detonation might have been a factor or if it just let go.
I might have missed this, do you run this thing on pump or e85? I'm certain it's in this thread somewhere, just curious. Haven't seen too many ringland failures so I'm kinda of surprised (but not really seeing how much abuse it has seen). Just curious if detonation might have been a factor or if it just let go.
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