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5000 RPM's at start!?

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Old Dec 5, 2012 | 09:22 AM
  #21  
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Thanks for all of the input guys. I Will check everything you guys mentioned this weekend.
Regarding the TB shaft pivot points, I did spray them down with some brake cleaner but it I didn't have this issue the first time I got the car running although I still had a relatively high idle (1300 rpm).

I blocked off both Egr holes on the intake manifold.

If I don't have a leak down tester can I just use a boost leak tester to pressurize the system?
Old Dec 5, 2012 | 10:02 PM
  #22  
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.

If I don't have a leak down tester can I just use a boost leak tester to pressurize the system?

Booster hose fitting or manifold side of PCV would both work. Just make sure the air line pressure regular is turned to 10 or 20 psi or less. You just need to listen for air flow and really don't need much pressure.
Old Dec 6, 2012 | 06:14 PM
  #23  
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If you have access to a smoke machine, that would be your best bet. Maybe they rent them?
Old Dec 7, 2012 | 01:12 PM
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Just wanted to add, 99 00 idle valve all the way open I saw high 4000s, close to 5k idle. Would rule that out if you haven't already.
Old Dec 15, 2012 | 03:43 PM
  #25  
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I dont know how I missed this. SMH BUT I am sooo relieved to have figured out the cause. Turns out I ordered the wrong year gasket.

Attached Thumbnails 5000 RPM's at start!?-imag0838.jpg  
Old Dec 15, 2012 | 04:31 PM
  #26  
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Same issue I had.

Thank god I am no longer the only retard on this forum.
Old Dec 15, 2012 | 11:02 PM
  #27  
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Originally Posted by Joe Perez
Manifold?
Originally Posted by Joe Perez
To get to 5,000 RPM, we are looking for LARGE leaks. Bigger than one of the small vacuum hoses or a tiny little gap around the EGR blockoff.
Originally Posted by Joe Perez
Maybe something got between the intake manifold and the head.
Originally Posted by Kinavo

Heh.

Glad you finally found the culprit.
Old Dec 16, 2012 | 10:11 AM
  #28  
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I was really hoping it wasnt the IM gasket but taking the manifold off wasnt as bad as I thought. I started the boost leak tester and there was absolutely no pressure building up. The other test I did was closing the throttle body and idle screw and the car still started and revved up to 4k. That's when I knew.
Old Dec 16, 2012 | 11:44 AM
  #29  
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Originally Posted by 240_to_miata
Thank god I am no longer the only retard on this forum.

post of the week.
Old Dec 16, 2012 | 01:30 PM
  #30  
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Why idle at 5000rpm?

Because racecar!!!!!!!
Old Dec 16, 2012 | 01:32 PM
  #31  
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Originally Posted by Braineack
post of the week.

x2
Old Dec 17, 2012 | 12:15 AM
  #32  
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hey, at least it was an error by the mechanic
Old Dec 22, 2012 | 05:22 PM
  #33  
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Car started fine today and idled at ~1500rpm for about 10 seconds. Thank you miataturbo folks. Still need to set the base timing and fix a coolant leak coming from the metal pipe coming from the heater core into the water pump outlet.

The real problem now is that Tunerstudio wont connect to the ECU all of a sudden. wth!
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