View Poll Results: Do we need a Subaru Subforum?
Yes! We need this!
0
0%
No! It's not a Miata and I don't care!
0
0%
Voters: 9001. You may not vote on this poll
The Dedicated URABUS Thread
#986
Elite Member
iTrader: (4)
Join Date: Aug 2009
Location: Redwood City, CA
Posts: 1,784
Total Cats: 42
Hit a deer on the way back from the beach. GG.
Hood, front bumper, headlights, and radiator support are done. it got pushed back so far it knocked the drive belt clean off the alternator lol. Hood scoop flew off and hit the car behind me -_-
Insurance is coming by to look at it right now actually. I don't really think its totaled since STIs are worth so much, but crossing my fingers anyway. None of the front suspension is tweaked or anything, everything structural besides the radiator support seems to be fine.
Hood, front bumper, headlights, and radiator support are done. it got pushed back so far it knocked the drive belt clean off the alternator lol. Hood scoop flew off and hit the car behind me -_-
Insurance is coming by to look at it right now actually. I don't really think its totaled since STIs are worth so much, but crossing my fingers anyway. None of the front suspension is tweaked or anything, everything structural besides the radiator support seems to be fine.
#989
Boost Czar
iTrader: (62)
Join Date: May 2005
Location: Chantilly, VA
Posts: 79,493
Total Cats: 4,080
I think my driver drain tube is clogged, but I can hear sloshing water after a rain when i brake/accelerate.
once i park it slowly drips down. Probably holds about a gallon of water--no joke.
meanwhile, clutch job is done. pretty damn easy job.
only two issues, one was we couldn't pop the driver ball joint and then we couldn't separate trans from block.
we decided to just unbolt the strut and that alone gave us enough room to pull the axles out. and for the trans it just took lots of wrestling--the dowel came out with the trans, so it was like rusted together.
once we put it all back together i just maxed my camber bolts. I can see a huge difference in how the tire sits on the ground now. off the sidewall.
clutch feel light and springy compared to last. Looks oem--exedy brand. My replacement kit looks identical. Im unsure why it went from feeling like a mustang clutch to a honda civic.
pro tip of the day. we removed the lower passenger stud on the block to put the trans back on. there's too much intereference with it and the turbo outlet to get it back on easy, once we removed that it went on like butter.
once i park it slowly drips down. Probably holds about a gallon of water--no joke.
meanwhile, clutch job is done. pretty damn easy job.
only two issues, one was we couldn't pop the driver ball joint and then we couldn't separate trans from block.
we decided to just unbolt the strut and that alone gave us enough room to pull the axles out. and for the trans it just took lots of wrestling--the dowel came out with the trans, so it was like rusted together.
once we put it all back together i just maxed my camber bolts. I can see a huge difference in how the tire sits on the ground now. off the sidewall.
clutch feel light and springy compared to last. Looks oem--exedy brand. My replacement kit looks identical. Im unsure why it went from feeling like a mustang clutch to a honda civic.
pro tip of the day. we removed the lower passenger stud on the block to put the trans back on. there's too much intereference with it and the turbo outlet to get it back on easy, once we removed that it went on like butter.
Last edited by Braineack; 03-29-2015 at 11:27 AM.
#993
Boost Czar
iTrader: (62)
Join Date: May 2005
Location: Chantilly, VA
Posts: 79,493
Total Cats: 4,080
I don't even joke around.
New clutch feels really good. I can't believe how much effort that last one took, the PP diaphragm springs must have been fubared or something. The ball of my foot would always get tired on the way home from work in stop and go. I suspect that I won't have that issue anymore.
Also, I was using that Scotty craptail mixture in my trans--I just went to 2 qts of BG synchro shift II and 2 qts of Mobil 1 synth and it feels like a brand new trans. Getting into reverse is what I'm really noticing is easier.
Very happy Braineack.
mmmm clutch dust:
New clutch feels really good. I can't believe how much effort that last one took, the PP diaphragm springs must have been fubared or something. The ball of my foot would always get tired on the way home from work in stop and go. I suspect that I won't have that issue anymore.
Also, I was using that Scotty craptail mixture in my trans--I just went to 2 qts of BG synchro shift II and 2 qts of Mobil 1 synth and it feels like a brand new trans. Getting into reverse is what I'm really noticing is easier.
Very happy Braineack.
mmmm clutch dust:
Last edited by Braineack; 03-30-2015 at 08:27 AM.
#996
2 Props,3 Dildos,& 1 Cat
iTrader: (8)
Join Date: Jun 2005
Location: Fake Virginia
Posts: 19,338
Total Cats: 573
meanwhile, clutch job is done. pretty damn easy job.
only two issues, one was we couldn't pop the driver ball joint and then we couldn't separate trans from block.
we decided to just unbolt the strut and that alone gave us enough room to pull the axles out. and for the trans it just took lots of wrestling--the dowel came out with the trans, so it was like rusted together.
once we put it all back together i just maxed my camber bolts. I can see a huge difference in how the tire sits on the ground now. off the sidewall.
clutch feel light and springy compared to last. Looks oem--exedy brand. My replacement kit looks identical. Im unsure why it went from feeling like a mustang clutch to a honda civic.
pro tip of the day. we removed the lower passenger stud on the block to put the trans back on. there's too much intereference with it and the turbo outlet to get it back on easy, once we removed that it went on like butter.
only two issues, one was we couldn't pop the driver ball joint and then we couldn't separate trans from block.
we decided to just unbolt the strut and that alone gave us enough room to pull the axles out. and for the trans it just took lots of wrestling--the dowel came out with the trans, so it was like rusted together.
once we put it all back together i just maxed my camber bolts. I can see a huge difference in how the tire sits on the ground now. off the sidewall.
clutch feel light and springy compared to last. Looks oem--exedy brand. My replacement kit looks identical. Im unsure why it went from feeling like a mustang clutch to a honda civic.
pro tip of the day. we removed the lower passenger stud on the block to put the trans back on. there's too much intereference with it and the turbo outlet to get it back on easy, once we removed that it went on like butter.
#999
Boost Czar
iTrader: (62)
Join Date: May 2005
Location: Chantilly, VA
Posts: 79,493
Total Cats: 4,080
because miata?
I only really used them to undo the DP to trans bracket. Otherwise, you didn't need anything but the standard extension.
oh yeah:
my DP was like hand tigntened onto the turbo. The gasket wasn't sealed and you could see that soot was exiting there.
It was coated in gasket maker too, so it makes me think the PO had a DP on the car at one point as well.
I had to spend at least 10min grinding off the gasket off the gasket and actually torqued down my DP bolts. In boost, I've noticed that the rattly noise by my turbo went away.
I love used cars.
I only really used them to undo the DP to trans bracket. Otherwise, you didn't need anything but the standard extension.
oh yeah:
my DP was like hand tigntened onto the turbo. The gasket wasn't sealed and you could see that soot was exiting there.
It was coated in gasket maker too, so it makes me think the PO had a DP on the car at one point as well.
I had to spend at least 10min grinding off the gasket off the gasket and actually torqued down my DP bolts. In boost, I've noticed that the rattly noise by my turbo went away.
I love used cars.