Notices
Build Threads Building a motor? Post the progress here.

sonofthehill sets his sights on MK ULTRA

Thread Tools
 
Search this Thread
 
Old Oct 19, 2017 | 12:13 AM
  #841  
sonofthehill's Avatar
Thread Starter
Elite Member
iTrader: (1)
 
Joined: Apr 2014
Posts: 3,199
Total Cats: 591
From: SF Bay Area, CA
Default

Cat got skunked tonight, washed him with hydrogen peroxide, baking soda, and dish detergent. He smells better than he has in years.

Well, that was exciting.

Also this for Aidan. The grommet is extended and paper thin on the one side. It was behind the road bike inner tube valve stem stem area, also hidden behind the mountain bike valve stem area between the can and bracket. I think the rod gets hot, so heat shields will only help so much. This did not use the double grommet in washer seals since it was my first attempt. It still sealed well, 40psi no problem.

Old Oct 21, 2017 | 05:05 PM
  #842  
Mobius's Avatar
Elite Member
iTrader: (2)
 
Joined: May 2008
Posts: 3,469
Total Cats: 365
From: Portland, Oregon
Default

Obviously we need a water sprayer for the rod.
Old Oct 21, 2017 | 08:29 PM
  #843  
sonofthehill's Avatar
Thread Starter
Elite Member
iTrader: (1)
 
Joined: Apr 2014
Posts: 3,199
Total Cats: 591
From: SF Bay Area, CA
Default

Nah, that's pansy sheyatch. I'm working on a heated hose to run my LN2 wastegate can cooling system. Yeah I'm gonna heat the cooling system line I just gotta make sure I don't freeze the grommet seals and somehow blow the chunks up my solenoid.

No I ain't gonna use it on my intercooler, might crack the thing.
Old Oct 21, 2017 | 11:46 PM
  #844  
sonofthehill's Avatar
Thread Starter
Elite Member
iTrader: (1)
 
Joined: Apr 2014
Posts: 3,199
Total Cats: 591
From: SF Bay Area, CA
Default

What is going on here? I have a new can that I put a big *** 245 kpa spring in, so the EBC is not on, this is wastegate only.

Is this compressor surge or possibly knock, or both?
Old Oct 22, 2017 | 11:28 AM
  #845  
sonofthehill's Avatar
Thread Starter
Elite Member
iTrader: (1)
 
Joined: Apr 2014
Posts: 3,199
Total Cats: 591
From: SF Bay Area, CA
Default

After thinking about it, I remembered that my pressure test didn't include the compressor housing. I think I will pull it and add a little sealant between the backing plate and housing. Then some sealant on the threads of the bolts.

This is driving me crazy, I don't understand why I can't have a solid MAP above 20 psi.
Old Oct 22, 2017 | 01:51 PM
  #846  
sonofthehill's Avatar
Thread Starter
Elite Member
iTrader: (1)
 
Joined: Apr 2014
Posts: 3,199
Total Cats: 591
From: SF Bay Area, CA
Default

Well, there's an o ring for the compressor on the large turbo, I haven't seen any on the smaller turbos. The 2 top bolts pass into the compressor housing, so I cleaned all the threads then filled the bolt threads with sealant. A little squeezed out between the bracket, the bolt heads and the housing, so we will see. Also put a smaller spring, so hopefully wastegate won't be in the oscillation zone anymore. Got that can so I can modify different aspects of it.
Here is a current picture
Old Oct 24, 2017 | 12:03 AM
  #847  
sonofthehill's Avatar
Thread Starter
Elite Member
iTrader: (1)
 
Joined: Apr 2014
Posts: 3,199
Total Cats: 591
From: SF Bay Area, CA
Default

The sealant on the bolt holes didn't make any difference so I thought about it more. I finally decided I need to put a check valve to my brake booster, I am gonna let Vlad give me 50 lashes with a wet noodle if this fixes it.
Old Oct 24, 2017 | 12:14 AM
  #848  
sonofthehill's Avatar
Thread Starter
Elite Member
iTrader: (1)
 
Joined: Apr 2014
Posts: 3,199
Total Cats: 591
From: SF Bay Area, CA
Default

Almost forgot, wine country is back in business so we are racing again starting this Wednesday. Hope to see some of you guys there, I am happy to help people learn how to make good launches, cut good lights, ect... With minimal tranny damage

This is my favorite corkscrew, self extracting, it's cool as hell.
I have to go to the dentist tomorrow (one of my favorite places,) so my wife brought home some alcohol to make me less unpleasant.
Old Oct 24, 2017 | 12:15 AM
  #849  
18psi's Avatar
VladiTuned
iTrader: (76)
 
Joined: Apr 2008
Posts: 35,821
Total Cats: 3,482
Default

lol I'm too tired to give lashes
Old Oct 24, 2017 | 12:17 AM
  #850  
sonofthehill's Avatar
Thread Starter
Elite Member
iTrader: (1)
 
Joined: Apr 2014
Posts: 3,199
Total Cats: 591
From: SF Bay Area, CA
Default



Oh well, I don't trust anyone else back there.
Old Nov 4, 2017 | 09:24 PM
  #851  
sonofthehill's Avatar
Thread Starter
Elite Member
iTrader: (1)
 
Joined: Apr 2014
Posts: 3,199
Total Cats: 591
From: SF Bay Area, CA
Default

So, I have been trying to eliminate possible causes of my boost oscillation. The check valve for the brake booster didn't make any difference, but I figured might as well not put additional stress on the booster so I left it.
Next, I eliminated my PCV valve and plugged the manifold, no difference so I put it back.
Today, I disconnected my boost gauge since I got it from Nigel way back for like $10 and he said it was a total POS, nothing.
I made a nice little 3/16 check valve today that I will use to isolate all the remaining vacuum devices/sensors from boost. We'll see.

The car is running well, tuning for max injector duty is actually quite comical. It's a freakin' insane, monstrous beast. I need fuel bad.
Old Nov 5, 2017 | 04:18 PM
  #852  
Art's Avatar
Art
Junior Member
 
Joined: Jul 2016
Posts: 369
Total Cats: -251
Default

.

Last edited by Art; Jun 11, 2018 at 05:05 PM.
Old Nov 5, 2017 | 10:38 PM
  #853  
sonofthehill's Avatar
Thread Starter
Elite Member
iTrader: (1)
 
Joined: Apr 2014
Posts: 3,199
Total Cats: 591
From: SF Bay Area, CA
Default

I did port the wastegate but I only opened the diameter on this one with minimal blending and smoothing. It holds a flat MAP signal up to about 20 psi. I am running the DIY "map daddy" sensor.
I stuck my check valve on the evap canister first, or whatever the frick that thing is. I need to get a good sustained high boost log to see, not just spinning through 2nd short into 3rd, hopefully it doesn't rain on Wednesday.
Old Nov 5, 2017 | 10:57 PM
  #854  
18psi's Avatar
VladiTuned
iTrader: (76)
 
Joined: Apr 2008
Posts: 35,821
Total Cats: 3,482
Default

I'm gonna do the same thing I do with the hundreds of wrx kids every day who "did a boost leak teast" on their car. Which in reality was just looking at their engine bay and saying "yup, doesn't leak".

Did you actually, smoke test for boost leaks? I just diagnosed a leaking intercooler last week. Leaking from the core. Just sayin
Old Nov 5, 2017 | 11:13 PM
  #855  
sonofthehill's Avatar
Thread Starter
Elite Member
iTrader: (1)
 
Joined: Apr 2014
Posts: 3,199
Total Cats: 591
From: SF Bay Area, CA
Default

Ok, I didn't do any smoke, but I did pump the thing up. I could have been more thuroug, how about a spray bottle with soapy water? I will cap it off again and do a better job tomorrow.
Old Nov 5, 2017 | 11:23 PM
  #856  
18psi's Avatar
VladiTuned
iTrader: (76)
 
Joined: Apr 2008
Posts: 35,821
Total Cats: 3,482
Default

I might be wrong thinking it's a leak, but even so, testing it again when you're preparing for man-boost could never hurt
Old Nov 5, 2017 | 11:26 PM
  #857  
patsmx5's Avatar
Elite Member
iTrader: (16)
 
Joined: Aug 2007
Posts: 9,406
Total Cats: 559
From: Houston, TX
Default

Try running 1 hose from the intercooler piping, directly to the wastegate. No boost solenoid inline whatsoever. See if the problem goes away.
Old Nov 5, 2017 | 11:39 PM
  #858  
sonofthehill's Avatar
Thread Starter
Elite Member
iTrader: (1)
 
Joined: Apr 2014
Posts: 3,199
Total Cats: 591
From: SF Bay Area, CA
Default

The solenoid is pretty restrictive. I will try that first, then recheck for leaks. I agree it doesn't hurt to check twice, plus I was basically checking around for hissing and my hearing isn't the best.
Old Nov 5, 2017 | 11:48 PM
  #859  
patsmx5's Avatar
Elite Member
iTrader: (16)
 
Joined: Aug 2007
Posts: 9,406
Total Cats: 559
From: Houston, TX
Default

I bet my suggestion fixes the oscillation.
Old Nov 7, 2017 | 02:42 PM
  #860  
sonofthehill's Avatar
Thread Starter
Elite Member
iTrader: (1)
 
Joined: Apr 2014
Posts: 3,199
Total Cats: 591
From: SF Bay Area, CA
Default

Vlad wins this round of find the problem with sonofthehill's car. Bypassing the solenoid made no difference, except that I have a bigger spring in there now.

My leaks are from the adjustment screw and the valve guide of my BOV. The screw was easy to see with soapy water, but I had to actually spray some into my BOV which I was a little hesitant to do. That's where it's coming from, it's pretty over complex and I think a little sealant between the main body and valve guide assembly, plus a few o rings will fix it.



All times are GMT -4. The time now is 02:03 PM.