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diy "turbo no hit block" '00 BP miata

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Old Feb 8, 2018 | 08:16 PM
  #581  
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Gross multi ground strap plugs are gross.
Old Feb 12, 2018 | 03:01 PM
  #582  
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Yesterday I opened bottom end to check for a strange clicking sound that varies with load, tured out main bearings are scratched, but the crank is good. Tomorrow new bearings will arrive, so I can install a new oil pump (old one was damaged)

Old Feb 12, 2018 | 06:31 PM
  #583  
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Can you shoot a picture of those scratched mains for reference? I had mains that developed a knock last year and pulled and replaced. The thing that was really surprising was how little damage there was. I didn't measure the gap back then, it must have simply been out of spec.

Any ideas for why you had scratched mains so soon after your new build? Insufficient cleaning? Didn't change the oil directly after a short run (20-30miles?)?
Old Mar 11, 2018 | 08:01 AM
  #584  
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Originally Posted by Mudflap
Can you shoot a picture of those scratched mains for reference? I had mains that developed a knock last year and pulled and replaced. The thing that was really surprising was how little damage there was. I didn't measure the gap back then, it must have simply been out of spec.

Any ideas for why you had scratched mains so soon after your new build? Insufficient cleaning? Didn't change the oil directly after a short run (20-30miles?)?
Sadly I trashed them, but IIRC they seemed ok, just out of spec (0.1mm every one)
Now I put a set of ACL race +0.25, the crank has to be machined by 0.20 instead of 0.25 to have 0.4mm of clearance, I also shaved the block to reach 0.8mm of quench and reassembled everything.
Result, after a street tune (dyno is busy until next week): it spins 4th gear, the power is good

Old Mar 11, 2018 | 11:41 AM
  #585  
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damn that looks like a fun powerband
Old May 4, 2018 | 12:27 PM
  #586  
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Another little update: some weeks ago I got a precision 600hp intercooler (this thing is HUGE) and a set of vs-855 volvo springs. Today I installed the springs with the engine installed (compressed air) but the difference in power was minimal (gained around 30whp) mainly because the internal wastegate of the efr seems to leak passed 20psi, so it's time to delete it and go external





I'm just concerned about the 600hp intercooler... seems really massive, I honestly doubt it will fit without any sorta of cut
Does anyone have pic of it installed?
Old May 5, 2018 | 07:59 PM
  #587  
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Today I managed to install the monster 600hp IC, it's a really tight fit, but it kinda fit.
no hopes to install the a/c condenser ever again, sadly...









Old Oct 14, 2018 | 10:28 AM
  #588  
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Sad to say, I'm parting out everything these days, the car will return stock
I've got no issues (except another 6spd gearbox, this time second gear exploded, and another r&p), the car runs like it has 420HP but it's time for me to turn back to naturally aspirated
sooo if anybody wants something I will be listing everything here in the classifields
Old Oct 14, 2018 | 10:31 AM
  #589  
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just to remember how it was, this video was made back when it dynoed 363 hp due to traction issues on the dyno
PS: the video was shot in mexico, of course
Old Oct 14, 2018 | 01:52 PM
  #590  
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NOOOOOO!!!! Don't partout!

PM me a price for the injectors if you must part everything out.
Old Oct 15, 2018 | 02:07 AM
  #591  
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It's a bummer to see this going south. Following this build was a big inspiration to me
Old Oct 27, 2018 | 12:29 PM
  #592  
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Aww, don't let the little green diff destroyer die! What are your plans? Thinking of getting an RX7 after all?
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