DIY Turbo Discussion greddy on a 1.8? homebrew kit?

diy "turbo no hit block" '00 BP miata

Thread Tools
 
Search this Thread
 
Old 02-08-2018, 08:16 PM
  #581  
Elite Member
iTrader: (1)
 
Leafy's Avatar
 
Join Date: Jun 2012
Location: NH
Posts: 9,479
Total Cats: 104
Default

Gross multi ground strap plugs are gross.
Leafy is offline  
Old 02-12-2018, 03:01 PM
  #582  
Junior Member
Thread Starter
 
DNA54's Avatar
 
Join Date: Nov 2013
Location: Sardinia, Italy
Posts: 396
Total Cats: 56
Default

Yesterday I opened bottom end to check for a strange clicking sound that varies with load, tured out main bearings are scratched, but the crank is good. Tomorrow new bearings will arrive, so I can install a new oil pump (old one was damaged)

DNA54 is offline  
Old 02-12-2018, 06:31 PM
  #583  
Junior Member
 
Mudflap's Avatar
 
Join Date: May 2017
Location: Louisville, Co
Posts: 466
Total Cats: 86
Default

Can you shoot a picture of those scratched mains for reference? I had mains that developed a knock last year and pulled and replaced. The thing that was really surprising was how little damage there was. I didn't measure the gap back then, it must have simply been out of spec.

Any ideas for why you had scratched mains so soon after your new build? Insufficient cleaning? Didn't change the oil directly after a short run (20-30miles?)?
Mudflap is offline  
Old 03-11-2018, 08:01 AM
  #584  
Junior Member
Thread Starter
 
DNA54's Avatar
 
Join Date: Nov 2013
Location: Sardinia, Italy
Posts: 396
Total Cats: 56
Default

Originally Posted by Mudflap
Can you shoot a picture of those scratched mains for reference? I had mains that developed a knock last year and pulled and replaced. The thing that was really surprising was how little damage there was. I didn't measure the gap back then, it must have simply been out of spec.

Any ideas for why you had scratched mains so soon after your new build? Insufficient cleaning? Didn't change the oil directly after a short run (20-30miles?)?
Sadly I trashed them, but IIRC they seemed ok, just out of spec (0.1mm every one)
Now I put a set of ACL race +0.25, the crank has to be machined by 0.20 instead of 0.25 to have 0.4mm of clearance, I also shaved the block to reach 0.8mm of quench and reassembled everything.
Result, after a street tune (dyno is busy until next week): it spins 4th gear, the power is good

DNA54 is offline  
Old 03-11-2018, 11:41 AM
  #585  
Senior Member
 
G3ML1NGZ's Avatar
 
Join Date: Aug 2012
Posts: 551
Total Cats: 101
Default

damn that looks like a fun powerband
G3ML1NGZ is offline  
Old 05-04-2018, 12:27 PM
  #586  
Junior Member
Thread Starter
 
DNA54's Avatar
 
Join Date: Nov 2013
Location: Sardinia, Italy
Posts: 396
Total Cats: 56
Default

Another little update: some weeks ago I got a precision 600hp intercooler (this thing is HUGE) and a set of vs-855 volvo springs. Today I installed the springs with the engine installed (compressed air) but the difference in power was minimal (gained around 30whp) mainly because the internal wastegate of the efr seems to leak passed 20psi, so it's time to delete it and go external





I'm just concerned about the 600hp intercooler... seems really massive, I honestly doubt it will fit without any sorta of cut
Does anyone have pic of it installed?
DNA54 is offline  
Old 05-05-2018, 07:59 PM
  #587  
Junior Member
Thread Starter
 
DNA54's Avatar
 
Join Date: Nov 2013
Location: Sardinia, Italy
Posts: 396
Total Cats: 56
Default

Today I managed to install the monster 600hp IC, it's a really tight fit, but it kinda fit.
no hopes to install the a/c condenser ever again, sadly...









DNA54 is offline  
Old 10-14-2018, 10:28 AM
  #588  
Junior Member
Thread Starter
 
DNA54's Avatar
 
Join Date: Nov 2013
Location: Sardinia, Italy
Posts: 396
Total Cats: 56
Default

Sad to say, I'm parting out everything these days, the car will return stock
I've got no issues (except another 6spd gearbox, this time second gear exploded, and another r&p), the car runs like it has 420HP but it's time for me to turn back to naturally aspirated
sooo if anybody wants something I will be listing everything here in the classifields
DNA54 is offline  
Old 10-14-2018, 10:31 AM
  #589  
Junior Member
Thread Starter
 
DNA54's Avatar
 
Join Date: Nov 2013
Location: Sardinia, Italy
Posts: 396
Total Cats: 56
Default


just to remember how it was, this video was made back when it dynoed 363 hp due to traction issues on the dyno
PS: the video was shot in mexico, of course
DNA54 is offline  
Old 10-14-2018, 01:52 PM
  #590  
Moderator
iTrader: (12)
 
sixshooter's Avatar
 
Join Date: Nov 2008
Location: Tampa, Florida
Posts: 20,664
Total Cats: 3,013
Default

NOOOOOO!!!! Don't partout!

PM me a price for the injectors if you must part everything out.
sixshooter is offline  
Old 10-15-2018, 02:07 AM
  #591  
Newb
 
tubitele's Avatar
 
Join Date: Dec 2011
Location: Slovenia
Posts: 28
Total Cats: 10
Default

It's a bummer to see this going south. Following this build was a big inspiration to me
tubitele is offline  
Old 10-27-2018, 12:29 PM
  #592  
Junior Member
 
ungluedflyer's Avatar
 
Join Date: Feb 2017
Location: Dallas, Texas
Posts: 100
Total Cats: 25
Default

Aww, don't let the little green diff destroyer die! What are your plans? Thinking of getting an RX7 after all?
ungluedflyer is offline  
Related Topics
Thread
Thread Starter
Forum
Replies
Last Post
Ridies
Ridies
0
12-08-2017 11:07 AM
MiataKeith
General Miata Chat
66
02-07-2014 05:08 PM
2manyhobyz
Media
5
07-25-2013 11:38 PM
BogusSVO
Useful Saved Posts
10
01-02-2013 01:15 PM
rappadan
Media
3
02-25-2009 02:38 AM



Quick Reply: diy "turbo no hit block" '00 BP miata



All times are GMT -4. The time now is 08:50 AM.