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Aidan's loose oily bunghole actually runs a track lap

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Old Feb 16, 2015 | 08:54 AM
  #481  
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Originally Posted by aidandj
In case you were wondering the 1.6 intake manifold gasket is NOT symmetrical. And it WILL leak coolant everywhere if installed backwards.



btw, that rowing **** looks like lots of fun (wonders if we have rowing teams in az).
Old Feb 16, 2015 | 09:59 AM
  #482  
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Originally Posted by Efini~FC3S
This thread sure is living up to its namesake...

Keep up the good work!
Its all a learning process. I am proud to say I haven't made the same mistake twice.

Originally Posted by hi_im_sean


btw, that rowing **** looks like lots of fun (wonders if we have rowing teams in az).
I'm sure it would be fun recreationally, but as a D1 sport it gets really tiring. We practice year round 6+ times a week. Just friday we had a 2k test in the morning, nothing like starting your day by throwing up twice and being oxygen deprived for the next 6 hours. I'm glad I'm a senior.
Old Feb 16, 2015 | 10:06 AM
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Yeah, rowing crew is hard core. You're basically taking the place of an internal combustion motor.
Old Feb 16, 2015 | 10:07 AM
  #484  
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Originally Posted by hornetball
Yeah, rowing crew is hard core. You're basically taking the place of an internal combustion motor.
It's all worth it when we actually go to race though. Also traveling to California and New Jersey on the schools dollar is pretty cool too
Old Feb 16, 2015 | 10:11 AM
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Update to the list:

To-Do:

0. FIND OIL LEAK/BURN
1. Inconel studs (RX-7 ordered, still need resbond but I think I am going to run without resbond for now because its a biatch to find)
2. Exhaust bracing. (Ordered a 3 inch exhaust clamp)
3. Locking downpipe bolts (Arrived)
4. Seats + Harness
4. Back braces (DIY)
5. Install new springs (550 Front, 350 rear)
6. Oil+water temp guages. (Going with a VEI systems gauge)
7. Helmet (Going to continue to run my open face helmet and wait for sa-2015)
8. Hardtop (Got one)
9. Put beads on intercooler pipes (Probably DIY: DIY $5 charge pipe bead roller - D-series.org, unless someone local knows somewhere to get it done cheap)
10. Find coolant leak. (risky to put this here but so far I haven't lost any coolant)
11. Find diff leak.
12. Heat Shielding. (master cylinder, brake lines)
13. Tune.
14. Break stuff.
15. Manifold relief cuts
Old Feb 16, 2015 | 11:21 AM
  #486  
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I have reached a new low. Wrench left on the crank pulley when I went to start it. Backed out the crank bolt in a few seconds.
Old Feb 16, 2015 | 11:27 AM
  #487  
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Hopefully it didn't hurt anything.

But, yeah, that's God telling you to take a day off.
Old Feb 16, 2015 | 11:32 AM
  #488  
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Ah Aidan... You do so much stuff I would do, ha.

So after tightening it again is it alive?
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Old Feb 16, 2015 | 11:34 AM
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What could have happened. I just tried to start it and it sounded tottally f'd up. Timing?
Old Feb 16, 2015 | 11:42 AM
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Fixed. Any guesses on why it sounded wrong? I'll give you a hint. I had just put it in gear to tighten the crank bolt.
Old Feb 16, 2015 | 11:43 AM
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Yes. It's quite possible that when the bolt loosened, the Woodruff key slipped/sheared/whatever. You should take the front apart and inspect/reverify/retorque everything. It'll go much faster this time!
Old Feb 16, 2015 | 12:03 PM
  #492  
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Old Feb 16, 2015 | 12:16 PM
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you sound like me when im in a hurry/excited/too many beers. slow down, take a break and go do some rows.

2nd video sounds like HLAs. they may take a while to "repump". if 10-20 minutes of idling-2k doesnt do it, id be throwing a pressure gauge on one of the head oil ports.

did you end up disassembling and cleaning them all?
Old Feb 16, 2015 | 12:17 PM
  #494  
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Originally Posted by aidandj
Fixed. Any guesses on why it sounded wrong? I'll give you a hint. I had just put it in gear to tighten the crank bolt.
im stumped
Old Feb 16, 2015 | 12:18 PM
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Yeah I was, I set **** down and cleaned for a bit. I soaked them in brake cleaner for a while, then soaked them in oil overnight.
Old Feb 16, 2015 | 12:18 PM
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Originally Posted by hi_im_sean
im stumped
I left it in gear. When I tried to start it it was trying to start against the e-brake...I need a break lol.
Old Feb 16, 2015 | 12:19 PM
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Originally Posted by aidandj
Yeah I was, I set **** down and cleaned for a bit. I soaked them in brake cleaner for a while, then soaked them in oil overnight.
so did you diassemble them? or did you just soak them assembled in each cocktail?
Old Feb 16, 2015 | 12:21 PM
  #498  
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Originally Posted by hi_im_sean
so did you diassemble them? or sis you just soak them assembled in each cocktail?
Nope. Did more reading and found people mostly just did it to get rid of the tick, and not actually for any other reason.
Old Feb 16, 2015 | 12:26 PM
  #499  
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Originally Posted by aidandj
Nope. Did more reading and found people mostly just did it to get rid of the tick, and not actually for any other reason.
hhhmmmm.

its possible some brake clean got into the hlas and didnt find its way out. not sure this is an issue, but i wouldnt have soaked them in a solvent without disassembly.
Old Feb 16, 2015 | 12:30 PM
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Originally Posted by hi_im_sean
hhhmmmm.

its possible some brake clean got into the hlas and didnt find its way out. not sure this is an issue, but i wouldnt have soaked them in a solvent without disassembly.
Hope not...



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